INTEGRATED COMPREHENSIVE ADJUSTMENT METHOD FOR PULVERIZED COAL BOILER BASED ON PREVENTION AND CONTROL OF HIGH-TEMPERATURE CORROSION OF WATER WALL

Information

  • Patent Application
  • 20230258328
  • Publication Number
    20230258328
  • Date Filed
    August 30, 2021
    3 years ago
  • Date Published
    August 17, 2023
    a year ago
Abstract
An integrated comprehensive adjustment method for a pulverized coal boiler based on high-temperature corrosion prevention and control of water wall is provided. The method includes: during shutdown period of the boiler, mounting reducing atmosphere sampling pipe on a water-cooled wall region; carrying out a diagnostic test on the boiler; carrying out an optimization and adjustment test of a boiler pulverizing system; carrying out a single-factor adjustment test of boiler-related parameters; determining degrees of influence of different parameters on water wall reducing atmosphere, thermal efficiency of the boiler and NOx concentration at a denitration inlet; carrying out an optimization test of ammonia spraying of a denitration system; carrying out a maximum safe denitration efficiency test; and finding a balance point among the water wall reducing atmosphere, the thermal efficiency of the boiler and the NOx concentration at the denitration inlet.
Description
FIELD OF TECHNOLOGY

The following relates to a combustion optimization and adjustment method for a pulverized coal boiler, in particular to an integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of the water wall.


BACKGROUND

High-temperature corrosion is a complex physical and chemical process in which the high temperature flue gas in the boiler interacts with the metal wall, and according to its mechanism, it can usually be divided into three categories: sulfate type high-temperature corrosion, sulfide type high-temperature corrosion and chloride type high-temperature corrosion; there are usually two types of high-temperature corrosion of domestic coal-fired boilers, namely sulfate type high-temperature corrosion and sulfide type high-temperature corrosion. The high-temperature corrosion on the water wall of coal-fired boilers is usually sulfide type high-temperature corrosion, which is mainly caused by H2S gas in the flue gas.


Due to the increasingly stringent environmental protection requirements, in order to control the emission of pollutants such as NON, coal-fired boilers generally adopt the low-nitrogen combustion technology of deep air classification, and there is oxygen-deficient combustion in the main combustion area of the boiler, so that a reducing atmosphere presents near the water wall of the boiler as a whole, the concentration of corrosive gases such as H2S increases, and the high-temperature corrosion of the boiler water wall becomes increasingly serious. At the same time, due to factors such as the difficulty of detecting H2S gas and the fact that high-temperature corrosion can only be found when the boiler is shut down for inspection, the problem of high-temperature corrosion of the boiler water wall is easily ignored during daily operation. In recent years, with the long-term operation of low-nitrogen combustion boilers and the implementation of stricter ultra-clean emission standards, the problem of high-temperature corrosion of boiler water walls has become increasingly prominent, and large-scale high-temperature corrosion and even pipe explosion of water walls have occurred from time to time, especially for boilers burning high-sulfur coal, the problem of high-temperature corrosion of the water wall is more prominent. The high-temperature corrosion of boiler water wall has become one of the main problems affecting the safe production of power plants.


At present, the measures to solve the problem of high temperature corrosion of boiler water wall mainly comprise combustion adjustment, use of low-sulfur coal for combustion, water wall spraying, anti-corrosion modification of wall wind, optimization of burner layout, etc., where, the boiler combustion adjustment is the first choice for many power plants when faced with high-temperature corrosion of water walls. However, the traditional combustion adjustment pays more attention to indicators such as the boiler steam temperature, the wall temperature, the content of combustible matter in fly ash, the exhaust gas temperature, the CO content, the boiler thermal efficiency and the NOx concentration, or is solely aimed at reducing the high-temperature corrosion of the water wall, it is impossible to realize the comprehensive optimization of the overall operation indicators of the boiler, that is, it is impossible to find the best balance between the safety, economic and environmental indicators such as the boiler water wall reducing atmosphere, the boiler thermal efficiency, the NOx concentration at the denitration inlet, and the steam temperature and wall temperature of the boiler.


SUMMARY

An aspect relates to an integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of the water wall, which can truly realize the comprehensive optimization of the overall operation indicators such as boiler water wall reducing atmosphere, the boiler thermal efficiency, and the NOx concentration at the denitration inlet.


To achieve the above purpose, a technical solution employed by the present disclosure is:


An integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of a water wall, comprises: mounting reducing atmosphere sampling pipes during a shutdown period to extract flue gas at the water wall of the boiler for testing; on this basis, obtaining key data such as water wall reducing atmosphere, NOx concentration at a denitration inlet, boiler thermal efficiency, steam temperature and wall temperature of the boiler, etc., through a comprehensive diagnostic test of the boiler and carrying out an adjustment test on the basis of this data; the present disclosure firstly carries out a basic optimization and adjustment test of the boiler pulverizing system, so as to carry out basic adjustment in terms of distribution of air powder and fineness of pulverized coal, so as to prevent the high-temperature corrosion of the water wall, the deviation of the steam temperature and the over temperature of the wall caused by the partial burning of the boiler; the present disclosure conducts the adjustment test of boiler-related adjustable parameters, and based on the test results, compares influence levels of the boiler-related parameters on the water wall reducing atmosphere, the boiler thermal efficiency, the NOx concentration at the denitration inlet, and the steam temperature and wall temperature of the boiler, to further determine priorities of the boiler-related parameters in the optimization process; after the optimization and adjustment of ammonia spraying, embodiments of the present invention determine a maximum value of NOx concentration at the denitration inlet that the denitration system can withstand under the condition that the ammonia escape does not exceed the standard, and then takes the maximum value of NOx concentration at the denitration inlet as a balance point of the NOx concentration at the denitration inlet, to determine a balance point between the boiler water wall reducing atmosphere and the boiler thermal efficiency, and according to the determined priority of the boiler-related parameters, determines an optimized operation mode of the boiler.


The present disclosure has the following beneficial effects:


Based on the integrated adjustment of pulverized coal-related parameters and boiler-related parameters, the present disclosure realizes the comprehensive optimization of the overall operation indicators such as boiler water wall reducing atmosphere, boiler thermal efficiency, and NOx concentration at the denitration inlet; this method can not only avoid the shortcomings of traditional combustion adjustment that only focuses on the indicators such as steam temperature, wall temperature, boiler thermal efficiency and NOx concentration at the denitration inlet, but ignores the problem of high-temperature corrosion of the water wall, but also avoid the shortcomings of the excessive consideration of the high-temperature corrosion of the water wall and neglecting the influence of boiler thermal efficiency and the NOx concentration index at the denitration inlet in the traditional combustion adjustment, especially the influence on the safe operation of the downstream equipment after the NOx concentration at the denitration inlet increases; the present disclosure obtains the best balance point between the safety, economy and environmental protection indicators such as the boiler water wall reducing atmosphere, the boiler thermal efficiency and the NOx concentration at the denitration inlet, and an optimized operation mode.





BRIEF DESCRIPTION

Some of the embodiments will be described in detail, with references to the following Figures, wherein like designations denote like members, wherein:



FIG. 1 is a schematic diagram of the overall flow of an embodiment;



FIG. 2a is the layout diagram of measuring points of reducing atmosphere near the water wall in this embodiment;



FIG. 2b is the layout diagram of measuring points of reducing atmosphere near the water wall in this embodiment;



FIG. 3a is the experimental result of adjusting the air distribution mode in this embodiment;



FIG. 3b is the experimental result of adjusting the air distribution mode in this embodiment;



FIG. 4a is the experimental result of adjusting the operation oxygen content in this embodiment;



FIG. 4b is the experimental result of adjusting the operation oxygen content in this embodiment;



FIG. 5a is the experimental result of adjusting the opening degree of the perimeter air in this embodiment;



FIG. 5b is the experimental result of adjusting the opening degree of the perimeter air in this embodiment;



FIG. 6 is the experimental result of adjusting the opening degree of the bypass air in this embodiment; and



FIG. 7 is the experimental result of changing the coal type in this embodiment.





DETAILED DESCRIPTION

In the following, the technical solutions of the present disclosure are explained clearly and completely below in conjunction with the accompanying drawings, and apparently, the described embodiments are merely a part of the embodiments of the present disclosure, not all the embodiments. Based on the embodiments of the present disclosure, all other embodiments obtained by one of ordinary skill in the conventional art without creative work fall within the protective scope of the present disclosure.


This embodiment takes the HG-2141/25.4-YM16 boiler manufactured by Harbin Boiler Factory Co., Ltd. as an example, and this boiler is a once-through boiler with primary intermediate reheat, at supercritical pressure variable pressure operation and configured with a built-in recirculation pump start-up system, and it is a π-type boiler with single furnace, balanced ventilation, solid slag tapping, full steel frame, full suspension structure and tight-fitting closed arrangement. Designed coal for the boiler is bituminous coal from Hequ County, Xinzhou City, Shanxi Province. The boiler adopts a cold primary air fan positive pressure direct blowing pulverizer system with double-in double-out steel ball mill, equipped with 6 sets of MGS3854 double-inlet and double-outlet steel ball mills, when the designed coal is used, 6 sets of coal mills are running, and there is no backup. The designed pulverized coal fineness R90 is 22.5%. The boiler adopts a novel tangential firing mode, the main burner is arranged on the four walls of the water wall, and each layer has 4 burners corresponding to a coal mill. SOFA burners are arranged at the four corners of the water wall above the main burner zone to achieve staged combustion to reduce NOx emissions. During the maintenance for the boiler, it was found that high-temperature corrosion occurred on the water wall pipes of the four walls of the boiler, the corrosion areas were mainly concentrated on the water wall pipes of the front wall and the rear wall, and the rear wall was the most serious. The high-temperature corrosion position of the water wall pipes is above the pulverized coal burners of the F layer of the main burners on the four walls of the boiler and below the high-level burnt-off air nozzles, and the total corrosion area is about 400 square meters.


Referring to FIG. 1, an integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of the water wall of this embodiment, comprises the following steps:


S1, During the shutdown period of the boiler, mounting reducing atmosphere sampling pipes on the water wall area of the boiler.


Specifically, in this step S1, inspection is carried out during the shutdown period, to determine the main area where high-temperature corrosion occurs on the water wall of the boiler; according to the furnace type and the area where high-temperature corrosion occurs, the installation distribution location and quantity of the reducing atmosphere sampling pipes are determined.


The boiler in this embodiment is a wall-type tangential-round boiler, and the high-temperature corrosion areas of the water wall are mainly concentrated on four walls above the pulverized coal burners of the F layer of the main burners on the four walls of the boiler and below the high-level burnt-off air nozzles. According to the furnace type, the area where the high-temperature corrosion of the water wall occurs, and the site conditions, the water wall reducing atmosphere sampling pipes are arranged in two layers in the height direction of the furnace, mainly distributed in the area between the burners of the F layer and SOFA air (a B-layer soot blower layer 2), the upper area of the SOFA air (a D-layer soot blower layer 1), each layer is provided with about 12 measuring points 3, and each side wall (the front wall 4, the rear wall 5, the left wall 6, and the right wall 7) is provided with 3 measuring points 3, a total of 24 measuring points in two layers. The arrangement of measuring points is shown in FIGS. 2a and 2b. The reducing atmosphere sampling pipes penetrate the furnace from the fins of the water wall and are flush with the inner wall of the water wall, and are stainless steel pipes with a diameter of about 10 mm.


S2. Carrying out a comprehensive diagnostic test of the boiler.


The test is carried out at three typical load points, namely high, medium and low load points, in this embodiment, the high load is a 570 MW load, the medium load is a 450 MW load, and the low load is a 300 MW load. During the test, the water wall reducing atmosphere, the NOx concentration at the denitration inlet, and the boiler thermal efficiency are mainly tested, and at the same time key data such as the boiler steam temperature and wall temperature in the DCS system are collected, so as to fully understand the facility operation status of the boiler, at the same time, the test parameter data obtained from the diagnostic test can be used as the basic data for the next adjustment test. The main results of the diagnostic test are shown in Table 1, and the results of the diagnostic test of the water wall reducing atmosphere are shown in Table 2.









TABLE 1







Summary of the results of the diagnostic test











Operating condition numbering

T-01
T-02
T-03





Operating condition description

570 MW load
300 MW load
450 MW load




diagnostic
diagnostic
diagnostic




operating
operating
operating


Load
MW
570.0
300.0
450.0


Mill operation mode

ABCDEF
BCEF
ABCDEF


Operation oxygen content on dashboard
%
2.60
4.70
3.60


Total amount of feeding coal
t/h
279
150
232


Ambient temperature
° C.
3
−2
2


NOx concentration at the denitration inlet on
mg/m3
272
281
288


dashboard
















Opening
UD
%
70
65
100


degree of
UC
%
10
0
30


air door
UB
%
70
40
80



UA
%
70
40
80



FF
%
45
40
45



F
%
45
40
45



EF
%
45
40
45



E
%
45
40
45



DE
%
45
40
45



D
%
45
30
45



DD
%
45
40
50



CC
%
45
40
50



C
%
60
40
50



BC
%
60
40
50



B
%
60
45
60



AB
%
65
40
60



A
%
65
20
60



AA
%
65
20
60


Air fan
Primary air fan current
A
181.0
140.0
164.0


current
Forced draft fan current
A
93.0
71.0
79.0



Induced draft fan current
A
441.0
286.0
360.0



Total fan current
A
715.0
497.0
603.0


Measured
Combustible matter in fly ash
%
0.97
0.39
0.66


data
Combustible matter in boiler slag
%
0.51
0.50
0.64



Operation oxygen content
%
2.87
4.99
3.68



NOx (6% O2)
mg/m3
288
295
303



CO content
μL/L
5
3
3


Boiler
Measured boiler thermal efficiency
%
93.08
92.65
93.17


thermal
Corrected exhaust gas temperature
° C.
144.2
135.1
139.7


efficiency
Corrected heat loss due to exhaust gas
%
5.91
6.23
5.95



Heat loss due to unburned carbon
%
0.50
0.21
0.33



Corrected boiler efficiency
%
93.09
92.90
93.16













Wall
Flue gas
SH finishing inlet
° C.
55
20
35


temperature
temperature
RH finishing inlet
° C.
7
64
28


and
deviation
RH finishing outlet
° C.
66
24
57


Steam
between two







temperature
sides of








furnace








outlet


















Maximum wall temperature of RH
° C.
596.2
583.6
594.9



finishing header







Maximum wall temperature of SH
° C.
604.1
605.4
604.3



finishing header







Maximum wall temperature of
° C.
531.6
533.7
527.5



division panel header







Maximum wall temperature of
° C.
415.6
391.2
400.1



vertical water wall







Main steam temperature
° C.
571.2/567.8
571.1/568.2
571.3/567.8



Reheat steam temperature
° C.
565.3/564.4
565.4/567.0
564.7/565.6



Main steam temperature deviation
° C.
3.4
2.9
3.5



on opposite sides







Reheat steam temperature
° C.
0.9
1.6
0.9



deviation on opposite sides
















TABLE 2





Test results of the water wall reducing atmosphere under different loads

















570 MW of diagnostic operating conditions,













the operation oxygen content is 2.6%, the





NOx concentration is 285 mg/m3,









Test

the sulfur content in coal is 0.73%












conditions

Front wall
Right wall
Rear wall
Left wall






















Measuring


Near

Near
Near

Near
Near

Near
Near

Near



point


left

right
front

rear
right

left
rear

front



positions
Items
Units
wall
Middle
wall
wall
Middle
wall
wall
Middle
wall
wall
Middle
wall
Mean





D-layer
O2
%
0.6
/
1.2
/
0.7
0.8
0.6
/
/
/
/
1.7
0.9


soot
CO
μL/L
30000
/
10600
/
11800
10800
16600
/
/
/
/
4151
13992


blower
H2S
μL/L
331
/
296
/
289
328
291
/
/
/
/
221
293


B-layer
O2
%
/
0.0
0.0
0.0
0.9
0.0
2.4
0.5
/
0.0
0.0
0.4
0.4


soot
CO
μL/L
/
61800
102400
46700
68000
53200
64500
10050
/
80800
10170
11000
69060


blower
H2S
μL/L
/
343
393
350
359
332
351
415
/
384
409
306
364












450 MW of basic operating conditions,













the operation oxygen content is 3.8%, the





NOxconcentration is 300 mg/m3,









Test

the sulfur content in coal is 0.76%












conditions

Front wall
Right wall
Rear wall
Left wall






















Measuring


Near

Near
Near

Near
Near

Near
Near

Near



point


left

right
front

rear
right

left
rear

front



positions
Items
Units
wall
Middle
wall
wall
Middle
wall
wall
Middle
wall
wall
Middle
wall
Mean





D-layer
O2
%
1.8
/
1.9
/
2.4
2.6
1.8
/
/
/
/
3.3
2.30


soot
CO
μL/L
6275
/
4383
/
1304
980
3555
/
/
/
/
356
2809


blower
H2S
μL/L
228
/
265
/
236
245
280
/
/
/
/
201
243


B-layer
O2
%
/
1.2
0.1
0.1
0.0
0.0
/
0.2
/
0.9
0.1
1.9
0.5


soot
CO
μL/L
/
1790text missing or illegible when filed
4650text missing or illegible when filed
6460text missing or illegible when filed
1026text missing or illegible when filed
91000
/
8420text missing or illegible when filed
/
1040text missing or illegible when filed
7650text missing or illegible when filed
6937
55626


blower
H2S
μL/L
/
326
355
384
406
399
/
412
/
351
394
299
370












300 MW of diagnostic operating conditions,













the operation oxygen content is 4.8%, the





NOx concentration is 282 mg/m3,









Test

the sulfur content of coal is 0.75%













conditions

Front wall
Right wall
Rear wall
Left wall























Measuring


Near

Near
Near

Near
Near

Near
Near

Near



point


left

right
front

rear
right

left
rear

front



positions
Items
Units
wall
Middle
wall
wall
Middle
wall
wall
Middle
wall
wall
Middle
wall
Mean





D-layer
O2
%
1.5
/
4.5
/
2.7
3.4
3.6
/
/
/
/
2.3
3.00


soot
CO
μL/L
1870
/
2455
/
4949
1710
6762
/
/
/
/
7613
7032


blower
H2S
μL/L
176
/
283
/
433
367
335
/
/
/
/
220
302


B-layer
O2
%
/
2.2
0.9
3.8
1.2
1.7
/
0.8
/
3.3
0.4
/
1.8


soot
CO
μL/L
/
6675
1690
3699
1320
12700
/
4250
/
1720
7640
/
23659


blower
H2S
μL/L
/
402
415
537
480
403
/
316
/
380
535
/
434





Note:


“/” means that there is air leakage in this measuring point, and the reducing atmosphere cannot be measured. It needs to eliminate the defect after the boiler is shut down.



text missing or illegible when filed indicates data missing or illegible when filed







S3, carrying out an optimization and adjustment test of the boiler pulverizing system.


In this test, the air-powder leveling test of the pulverized coal pipe of the coal mill is first carried out; whether the primary air-powder of each pulverized coal pipe at the outlet of the coal mill is uniform directly affects the combustion condition in the furnace. When the difference between the primary air-powder in the pulverized coal pipe is too large, it will cause problems such as combustion deflection, over-temperature of the local water wall pipe wall, and clogging of the pulverized coal pipe. By adjusting the adjustable shrinkage hole of the coal mill and the pulverized coal distributor, the air velocity deviation between the pulverized coal pipes of the coal mill is controlled within 5%, and the deviation of the pulverized coal amounts between two pulverized coal pipes on the same side of the coal mill is also controlled within 5%, to achieve uniform air-powder distribution.


Secondly, the fineness adjustment test of the pulverized coal of the coal mill is carried out. In the conventional blended coal combustion mode of the boiler, the weighted volatile Vdaf of the burning blended coal is about 40%˜43%, and the reasonable pulverized coal fineness R90 should be about 20.0%˜25.5%. Through the diagnostic test of the pulverized coal fineness of each coal mill, it can be seen that the pulverized coal fineness R90 of the coal mills A, C, D, and F is about 17.0%˜20.0%, and the pulverized coal fineness R90 of the coal mill B and E s is about 14.0%˜17.0%. In order to increase the coal mill output, the pulverized coal fineness of the coal mill is properly adjusted by a damper of a folding door, and after the adjustment, the output of a single coal mill is increased by about 2 t/h˜3 t/h, and the pulverized coal fineness R90 of all coal mill is in the range of 20% to 25.5%, and the adjustment results are shown in Table 3.









TABLE 3





Summary of pulverized coal fineness of coal mills after adjustment



















Coal mills
Units
Mill A
Mill B
Mill C





Feeding coal amount
t/h
23/23
21/21
25/25














Pulverized coal pipe

#1/#3 side
#2/#4 side
#1/#3 side
#2/#4 side
#1/#3 side
#2/#4 side


Opening degree of

1.0
2.0
1.5
2.5
2
3


damper of folding door









Pulverized coal
%
23.0
22.6
25.8
24.9
21.0
19.6














Coal mills
Units
Mill D
Mill E
Mill F





Feeding coal amount
t/h
22/22
21/21
19/19














Pulverized coal pipe

#1/#3 side
#2/#4 side
#1/#3 side
#2/#4 side
#1/#3 side
#2/#4 side


Opening degree of

2.5
2.5
2.0
1.5
1.7
1.7


damper of folding door









Pulverized coal
%
24.6
25.2
23.3
24.1
21.3
20.9









S4, Carrying out a single-factor adjustment test of boiler-related parameters.


The boiler-related parameters of the single-factor adjustment test in step S4 mainly comprises the air distribution mode, the opening degree of perimeter air, the primary air velocity, the operation oxygen content, and the coal sulfur content; the single-factor adjustment test can measure the water wall reducing atmosphere, the boiler thermal efficiency, and the NOx concentration at the denitration inlet according to the adjustment of the boiler-related parameters, and carry out statistics of the boiler steam temperature and wall temperature.


1) Adjustment Test of the Air Distribution Mode:


The air distribution adjustment test was carried out under the load of 550 MW and 300 MW, and the test results of the water wall reducing atmosphere in the area between the burners and the burnt-off air, the NOx concentration (6% O2) at the denitration inlet and the boiler thermal efficiency under different air distribution modes are shown in FIGS. 3a and 3b. It can be seen from the test results that as the proportion of burnt-off air decreases, the H2S content of the water wall in the area between the burners and the burnt-off air decreases, the boiler thermal efficiency does not change much, but the NOx concentration at the denitration inlet increases;


2) Adjustment Test of the Operation Oxygen Content:


Under the condition that other operating parameters are the same for 550 MW and 300 MW loads, the operation oxygen content adjustment test was carried out, and the test results of the water wall reducing atmosphere in the area between the burners and the burnt-off air, the NOx concentration (6% O2) at the denitration inlet and the boiler thermal efficiency under different operation oxygen contents are shown in FIGS. 4a and 4b. It can be seen from the test results that as the proportion of operation oxygen content increases, the H2S content of the water wall in the area between the burners and the burnt-off air decreases, but the boiler thermal efficiency decreases, and the NOx concentration at the denitration inlet increases.


3) Adjustment Test of the Opening Degree of the Perimeter Air:


Under the operation conditions of 490 MW and 300 MW, the opening degrees of the air door of the perimeter air were respectively adjusted from 40% to 25% and 60%, to carry out the adjustment test of the opening degree of the perimeter air, and the test results are shown in FIGS. 5a and 5b. From the results of the adjustment test of the perimeter air, it can be seen that, although decreasing of the opening degree of the air door of the perimeter air will reduce the NOx content at the denitration inlet, the combustible content in fly ash will increase, the boiler thermal efficiency will decrease, and at the same time, the H2S content on the water wall reducing atmosphere will increase. Therefore, during daily operation, the opening degree of the perimeter air should be controlled within the range of 40% to 60%.


4) Adjustment Test of the Primary Air Velocity:


Under the conditions of 300 MW load, the same air distribution mode, and the same operation oxygen content, the opening degree of the bypass air of the four coal mills in operation was opened from 25% to 35%, and the primary air velocity of the pulverized coal pipe was increased from about 24 m/s to 27.5 m/s. The test results of the water wall reducing atmosphere in the area between the burners and the burnt-off air, the NOx concentration (6% O2) at the denitration inlet and the boiler thermal efficiency under different opening degrees of the bypass air are shown in FIG. 6. It can be seen from the test results that the opening degree of the bypass air and the primary air velocity of the pulverized coal pipe have little effect on indicators such as the boiler thermal efficiency, the NOx content at the denitration inlet, and the H2S content on the water wall. According to the test results of the bypass air, the opening degree of the bypass air remains in the current control state.


5) Test of Changing the Coal Type (Sulfur Content in Coal):


According to the actual coal combustion situation of the power plant, two coal types with sulfur content of 0.73% and 0.97% were selected to test the concentration of reducing gas on the water wall area of the furnace, so as to compare the influence of the change of sulfur content in the coal quality on the reducing atmosphere. The results are shown in FIG. 7. It can be seen from the test results that with the increase of the sulfur content in the coal, the H2S content in the flue gas near the water wall of the furnace shows an overall upward trend, and the amount of slag in the furnace increases, and the temperature of the buffer slag hopper increases. Therefore, from the consideration of alleviating the high-temperature corrosion and dropping coke of the water wall in the furnace, low-sulfur coal with a sulfur content of 0.73% is used in daily operation. S5, Determining the influence levels of the different parameters on the water wall reducing atmosphere, the boiler thermal efficiency, the NOx concentration at the denitration inlet, and the steam temperature and wall temperature of the boiler, to determine the priorities of the respective relevant parameters in the optimization process.


From the test results of step S4, it can be seen that, although decreasing of the opening degree of the air door of the perimeter air will reduce the NOx content at the denitration inlet, the combustible content in fly ash will increase, the boiler thermal efficiency will decrease, and at the same time, the H2S content on the water wall reducing atmosphere will increase. The opening degree of the bypass air and the primary air velocity of the pulverized coal pipe have little effect on indicators such as the boiler thermal efficiency, the NOx content at the denitration inlet, and the H2S content on the water wall.


In order to reduce the H2S content in the flue gas near the water wall, methods such as increasing the operation oxygen content and reducing the proportion of burnt-off air can be adopted, but the above methods will lead to an increase in the NOx concentration at the denitration inlet. Turning down the air door of the burnt-off air will reduce the H2S content in the flue gas near the water wall, but increase the NOx concentration at the denitration inlet, and has little effect on the power consumption of the fan and the boiler thermal efficiency. Compared with increasing the operation oxygen content, turning down the air door of the burnt-off air will also increase the NOx concentration at the denitration inlet, but it has little effect on the boiler economic efficiency, therefore, the adjustment of air distribution mode is chosen as a measure to slow down the high-temperature corrosion of the water wall.


S6, Carrying out an optimization test of ammonia spraying of the denitration system.


Under the load of the unit ranged from 300 MW to 570 MW, according to the NOx concentration distribution at a reactor outlet, the manual valve opening of each branch pipe of the AIG ammonia spraying grid was optimized and adjusted for multiple rounds. After the optimization and adjustment of ammonia spraying, the NOx concentration distribution at the SCR outlet maintains a good uniformity under different unit loads, and the local ammonia spraying amount matches the NOx concentration distribution. Wherein, under the unit load of 570 MW, when the NOx concentrations at the SCR inlet and outlet are about 318 mg/m3 and 36 mg/m3, respectively, the relative standard deviation CV values of the NOx concentration distribution at the reactor outlet of A and B sides are 13% and 15%, respectively, and the average ammonia escape concentrations were 1.7 μL/L and 2.4 μL/L, respectively.


S7, carrying out the maximum safe denitration efficiency test to determine the maximum inlet NOx concentration value that the denitration system can withstand.


On basis of step S6, the maximum safe denitration efficiency test was carried out. Under the current high load of the unit, the potential P of the SCR denitration reactor is about 2.79, and under the condition that the ammonia escape concentration is 3 μL/L, the maximum safe denitration efficiency is about 89.0%, and under the condition that the ammonia escape does not exceed standard, if the NOx concentration at the denitration outlet is controlled to be 40 mg/m3, the maximum NOx concentration at the denitration inlet that the denitration system inlet can withstand is about 366 mg/m3.


S8, Finding the best balance point among the safety, economy, and environmental protection indicators such as the boiler water wall reducing atmosphere, the boiler thermal efficiency, and the NOx concentration at the denitration inlet, and determining the optimized operation mode of the boiler.


According to the test results of step S5, in order to reduce the H2S content in the flue gas near the water wall, it will inevitably cause an increase in the NOx concentration at the denitration inlet. The increase in the NOx concentration at the denitration inlet will cause problems such as an increase in the amount of ammonia spraying, an increase in ammonia escape, and an increase in the risk of ammonium bisulfate blockage in downstream equipment. According to the test results of the denitration system, if the NOx concentration at the denitration inlet does not exceed 366 mg/m3, and the ammonia escape at the denitration outlet basically does not exceed the specified standard of 3 μL/L, the risk of ammonium bisulfate blockage in downstream equipment is relatively low. Then, the increased cost of increasing the NOx concentration at the denitration inlet to control the water wall reducing atmosphere is mainly the cost of increasing the amount of ammonia spraying.


Through the estimation, it can be seen that, if the control value of NOx concentration at the denitration inlet increases by 50 mg/m3, and the annual increase of liquid ammonia cost is about 650,000 yuan, and the calculation results are shown in Table 4.









TABLE 4







Estimation of the effect of the increase in NOx concentration


at the denitration inlet on the annual liquid ammonia cost












Current control value of
NOx concentration at the




NOx at the denitration
denitration inlet


Item name
Units
inlet
increased by 50 mg/m3













Unit load
MW
570
570


Total flue gas amount
m3/h
1930481
1931530


NOx emission concentration at the
mg/m3
290
340


denitration inlet


Ammonia consumption
kg/h
182
218


Annual utilization hours of the unit
h
5200
5200


Annual ammonia consumption
t/year
949
1135


Liquid ammonia price
Yuan/t
3500
3500


Annual liquid ammonia
Ten thousand
332
397


consumption cost
yuan


Annual increase in liquid ammonia
Ten thousand

65


consumption cost
yuan









Considering the high-temperature corrosion of the water wall, the increased cost of liquid ammonia and the possible impact on other equipment, it is recommended to increase the current control value of NOx concentration at the denitration inlet by 50 mg/m3, that is, from 270 mg/m3˜300 mg/m3 to 320 mg/m3˜350 mg/m3.


After determining the balance point of the NOx concentration at the denitration inlet, the final optimized operation mode such as the air distribution mode, the operation oxygen content could be determined, so that the best balance point among the safety, economy, and environmental protection indicators such as the boiler water wall reducing atmosphere, the boiler thermal efficiency, and the NOx concentration at the denitration inlet, and the optimized operation mode of the boiler are obtained.


The results of optimized operating conditions under different loads are shown in Table 5, wherein:


1) Under the load of 570 MW−300 MW, through adjustment, the H2S content of the reducing atmosphere near the water wall in the area between the burners and the burnt-off air (the B-layer soot blower layer) can be reduced by about 50 μL/L˜123 μL/L, with a decrease of about 14% to 28%. The reducing atmosphere near the water wall is significantly reduced, which greatly alleviates the problem of high-temperature corrosion of the water wall and reduces the risk of pipe explosion in the boiler;


2) After adjustment, there is no significant change in boiler thermal efficiency under different loads.


3) After adjustment, the control value of NOx concentration at the denitration inlet increases by 50 mg/m3, and the annual increase of liquid ammonia cost is about 650,000 yuan.


4) After adjustment, the pipe wall temperature of the finishing-superheater is reduced by 4° C. 6° C., reducing the risk of overheating of the heating surface pipe wall.


Through the integrated comprehensive adjustment method, a reasonable balance point of taking into account the safety, economy and environmental protection of the boiler is found, and the optimized operation mode suitable for the operation of the boiler is obtained. The optimized air distribution mode and content control function for operation oxygen are shown in Table 6 and Table 7.









TABLE 5







Summary of the results of optimized operating conditions under different loads














Operating condition

T-01
T-72
T-59
T-64
T-47
T-58





Operating condition description

570 MW
550 MW
450 MW
450 MW
300 MW
300 MW




load
load
load
load
load
load




diagnostic
optimized
diagnostic
optimized
diagnostic
optimized


Load
MW
570.0
550.0
450.0
450.0
300.0
300.0


Mill operation mode

ABCDEF
ABCDEF
ABCDEF
ABCDEF
BCEF
BCEF


Operation oxygen
%
2.60
2.90
3.80
4.20
5.00
5.10


content on dashboard









Total amount of
t/h
279
270
224
218
164
160


Ambient temperature
° C.
3
−3
2
−4
−9
2


NOx concentration at
mg/m3
272
343
295
350
286
349


the denitration inlet






















Opening
UD
%
70
60
100
70
80
60


degree
UC
%
10
0
0
0
10
0


of air
UB
%
70
50
80
50
60
30


door
UA
%
70
50
80
50
60
30



FF
%
45
20/40/40/6
20/40/40/6
25/40/40/4
40
40



F
%
45
20/40/40/6
20/40/40/6
25/40/40/4
40
60



EF
%
45
20/40/40/6
20/40/40/6
25/40/40/4
40
40



E
%
45
45
45
40
40
60



DE
%
45
45
45
40
40
40



D
%
45
45
45
40
30
30



DD
%
45
45
50
40
40
40



CC
%
45
45
50
40
40
40



C
%
60
60
50
40
40
60



BC
%
60
60
50
45
40
45



B
%
60
60
50
45
40
60



AB
%
65
65
55
45
40
45



A
%
65
65
55
45
20
20



AA
%
65
65
55
45
20
20


Air fan
Primary air
A
181.0
177.0
171.0
161.0
145.0
147.0


current
fan current










Forced draft
A
93.0
90.0
80.0
79.0
73.0
71.0



fan current










Induced
A
441.0
422.0
361.0
358.0
294.0
294.0



draft fan










current










Total fan
A
715.0
689.0
612.0
598.0
512.0
512.0


Measured
Combustible
%
0.97
0.85
0.51
0.41
0.58
0.63


data
matter in fly










ash










Combustible
%
0.51
0.49
0.21
0.22
0.67
0.25



matter in










boiler slag










Operation
%
2.87
3.05
4.03
4.43
5.55
5.40



oxygen










content










NOx (6%
mg/m3
288
370
313
375
302
368



O2)










CO content
μL/L
5
4
8
3
4
3


Boiler
Measured
%
93.08
92.85
92.85
92.97
92.60
92.59


thermal
boiler









efficiency
thermal










efficiency










Corrected
° C.
144.2
142.3
139.1
136.7
131.9
134.2



exhaust gas










temperature










Corrected
%
5.91
5.86
6.04
6.03
6.22
6.28



heat loss due










to exhaust










gas










Heat loss
%
0.50
0.23
0.23
0.20
0.29
0.29



due to










unburned










carbon










Corrected
%
93.09
93.21
93.18
93.21
92.83
92.77



boiler










efficiency























Wall
Flue gas
SH
° C.
55
50
79
35
69
45


temperature
temperature
finishing









and
deviation
inlet









steam
between
RH
° C.
7
10
17
50
76
76


temperature
two
finishing










sides of
inlet










furnace











outlet












RH
° C.
66
73
72
53
15
5




finishing











outlet























Maximum
° C.
596.2
590
589.2
585.3
591.2
579.6



wall










temperature










Maximum
° C.
604.1
598.9
600.6
598.2
604.2
596.5



wall










temperature










Maximum
° C.
531.6
525.7
539.3
531.8
531.8
527.7



wall










temperature










Maximum
° C.
415.6
419.7
406.1
404.3
386.7
378.8



wall










Main steam
° C.
571.2/567.text missing or illegible when filed
569.4/566.text missing or illegible when filed
569.1/567.text missing or illegible when filed
572.1/567.text missing or illegible when filed
571.9/568.text missing or illegible when filed
571.7/567.text missing or illegible when filed



Reheat
° C.
565.3/564.text missing or illegible when filed
566.8/563.text missing or illegible when filed
565.8/562.text missing or illegible when filed
566.7/564.text missing or illegible when filed
565.9/570.text missing or illegible when filed
564.7/563.text missing or illegible when filed



Main steam
° C.
3.4
2.8
2.1
4.8
3.8
4.2



temperature










deviation on










Reheat
° C.
0.9
3.1
3.1
2.1
4.2
1.2



steam










temperature









Flue gas
O2 at D-
%
0.9
1.5
2.3
2.8
3.0
3.9


composition
layer soot









near
blower layer









the
CO at D-
μL/L
13992
6542
2809
2293
7032
686


water
layer soot









wall
blower layer










H2S at D-
μL/L
293
246
243
228
302
194



layer soot










blower layer










O2 at B-
%
0.4
0.4
0.5
0.7
1.8
2.1



layer soot










blower layer










CO at B-
μL/L
69060
41656
55626
24760
23659
13041



layer soot










blower layer










H2S at B-
μL/L
364
313
370
316
434
311



layer soot










blower layer






text missing or illegible when filed indicates data missing or illegible when filed














TABLE 6







Recommended air distribution mode under different loads













Air doors
Units
600 MW
450 MW
300 MW

















UD layer
%
60
60
60



UC layer
%
0
0
0



UB layer
%
50
40
30



UA layer
%
50
40
30



FF layer
%
40
40
40



F layer
%
40
40
40



EF layer
%
40
40
40



E layer
%
40
40
40



DE layer
%
40
40
40



D layer
%
50
50
30



DD layer
%
50
50
40



CC layer
%
50
50
50



C layer
%
60
50
50



BC layer
%
60
50
50



B layer
%
60
50
50



AB layer
%
60
55
50



A layer
%
60
55
10



AA layer
%
60
55
10

















TABLE 7





Optimized boiler operation oxygen content control value























Current
Load command, MW
300
350
400
450
500
550
600


control value
Operation oxygen
4.80
4.47
4.13
3.80
3.37
2.93
2.50



content, %









Recommended
Load command, MW
300
350
400
450
500
550
600


control value
Operation oxygen
4.8
4.47
4.13
4.00
3.57
3.13
2.70



content, %









Although the present invention has been disclosed in the form of embodiments and variations thereon, it will be understood that numerous additional modifications and variations could be made thereto without departing from the scope of the invention.


For the sake of clarity, it is to be understood that the use of ‘a’ or ‘an’ throughout this application does not exclude a plurality, and ‘comprising’ does not exclude other steps or elements.

Claims
  • 1. An integrated comprehensive adjustment method for a pulverized coal boiler based on prevention and control of high-temperature corrosion of a water wall, the method comprising: S1, during a shutdown period of the boiler, mounting reducing atmosphere sampling pipes on the water wall area of the boiler;S2, carrying out a comprehensive diagnostic test of the boiler;S3, carrying out an optimization and adjustment test of a boiler pulverizing system;S4, carrying out a single-factor adjustment test of boiler-related parameters;S5, determining a degree of an influence of different parameters on water wall reducing atmosphere, boiler thermal efficiency, and NOx concentration at a denitration inlet;S6, carrying out an optimization test of ammonia spraying of a denitration system;S7, carrying out a maximum safe denitration efficiency test to determine a maximum value of NOx concentration at the denitration inlet that the denitration system can withstand; andS8, finding a best balance point between the water wall reducing atmosphere of the boiler, the boiler thermal efficiency, and the NOx concentration at the denitration inlet, and determining an optimized operation mode of the boiler.
  • 2. The integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of a water wall according to claim 1, in step S1, during the shutdown period, carrying out inspection to determine main area where high-temperature corrosion occurs on the water wall of the boiler; according to a furnace type and an area where high-temperature corrosion occurs, determining the installation distribution location and quantity of the reducing atmosphere sampling pipes.
  • 3. The integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of a water wall according to claim 2, wherein the reducing atmosphere sampling pipes penetrate a furnace from fins of the water wall and are flush with an inner wall of the water wall of the boiler when mounting the reducing atmosphere sampling pipes.
  • 4. The integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of a water wall according to claim 1, in step S2, test data for the diagnostic test comprises the water wall reducing atmosphere, the NOx concentration at the denitration inlet, the boiler thermal efficiency, a steam temperature of the boiler, and a wall temperature.
  • 5. The integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of a water wall according to claim 1, wherein the comprehensive diagnostic test in step S2 is carried out at three typical load points, the three typical load points being a high load point, a medium load point and a low load point.
  • 6. The integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of a water wall according to claim 1, wherein the optimization and adjustment test in step S3 comprises an air-powder leveling test of a pulverized coal pipe of a coal mill, and a fineness optimization test of the pulverized coal of the coal mill; the air-powder leveling test of the pulverized coal pipe of the coal mill and the fineness optimization test of the pulverized coal of the coal mill are carried out in sequence.
  • 7. The integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of a water wall according to claim 6, during the air-powder leveling test of the pulverized coal pipe of the coal mill, by adjusting an adjustable shrinkage hole of the coal mill and a pulverized coal distributor, air velocity deviation between the pulverized coal pipes of the coal mill is controlled within 5%, and deviation of the pulverized coal amounts between the two pulverized coal pipes on the same side of the coal mill is also controlled within 5%.
  • 8. The integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of a water wall according to claim 6, during the fineness optimization test of the pulverized coal of the coal mill, pulverized coal fineness of the coal mill is adjusted by a damper of a folding door, and the pulverized coal fineness of all coal mill is in a range of 20% to 25.5% thereby.
  • 9. The integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of a water wall according to claim 1, wherein the boiler-related parameters of the single-factor adjustment test in step S4 comprises air distribution mode, opening degree of perimeter air, primary air velocity, operation oxygen content, and sulfur content in coal; the single-factor adjustment test measures the water wall reducing atmosphere, the boiler thermal efficiency, and the NOx concentration at the denitration inlet according to the adjustment of the boiler-related parameters, and statistics of the boiler steam temperature and wall temperature is carried out.
  • 10. The integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of a water wall according to claim 1, in step S5, according to the single-factor adjustment test in step S4, comparing influence levels of the boiler-related parameters on the water wall reducing atmosphere, the boiler thermal efficiency, and the NOx concentration at the denitration inlet, and determining priorities of the respective related parameters in an optimization process.
  • 11. The integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of a water wall according to claim 10, in step S8, taking the maximum value of NOx concentration at the denitration inlet that the denitration system can withstand as a balance point of the NOx concentration at the denitration inlet, to determine the balance point between the water wall reducing atmosphere of the boiler and the boiler thermal efficiency, and according to the determined priorities of the boiler-related parameters in step S5, determining the optimized operation mode of the boiler.
  • 12. The integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of a water wall according to claim 1, in step S6, under different load operating conditions, according to NOx concentration distribution at an outlet section of an SCR reactor, adjusting ammonia flows of branch pipes of each ammonia spraying grid, to cause local ammonia spraying amount to match the NOx concentration distribution.
  • 13. The integrated comprehensive adjustment method for a pulverized coal boiler based on the prevention and control of high-temperature corrosion of a water wall according to claim 1, in step S7, finding out a maximum safe denitration efficiency corresponding to the high load through test, and under the condition that the ammonia escape does not exceed standard, determining the maximum value of NOx concentration at the denitration inlet that the denitration system can withstand;
  • 14. An integrated comprehensive adjustment method for a pulverized coal boiler based on prevention and control of high-temperature corrosion of a water wall, S1, during a shutdown period of the boiler, mounting reducing atmosphere sampling pipes on the water wall area of the boiler; first determining main area where high-temperature corrosion occurs on the water wall of the boiler, then according to a furnace type and an area where high-temperature corrosion occurs, determining an installation distribution location and quantity of the reducing atmosphere sampling pipes, and the reducing atmosphere sampling pipes penetrate a furnace from fins of the water wall and are flush with an inner wall of the water wall of the boiler when mounting the reducing atmosphere sampling pipes;S2, carrying out a comprehensive diagnostic test of the boiler; the comprehensive diagnostic test is carried out at three typical load points, the three typical load points being a high load point, a medium load point, and a low load point, and test data comprises the water wall reducing atmosphere, the NOx concentration at the denitration inlet, a boiler thermal efficiency, a steam temperature of the boiler, and a wall temperature;S3, carrying out an optimization and adjustment test of a boiler pulverizing system; the test in step S3 comprises an air-powder leveling test of a pulverized coal pipe of a coal mill, and a fineness optimization test of the pulverized coal of the coal mill; the air-powder leveling test of the pulverized coal pipe of the coal mill and the fineness optimization test of the pulverized coal of the coal mill are carried out in sequence, wherein: during the air-powder leveling test of the pulverized coal pipe of the coal mill, by adjusting an adjustable shrinkage hole of the coal mill and a pulverized coal distributor, air velocity deviation between the pulverized coal pipes of the coal mill is controlled within 5%, and deviation of the pulverized coal amounts between the two pulverized coal pipes on a same side of the coal mill is also controlled within 5%, and during the fineness optimization test of the pulverized coal of the coal mill, pulverized coal fineness of the coal mill is adjusted by a damper of a folding door, and the pulverized coal fineness of all coal mill is in a range of 20% to 25.5% thereby;S4, carrying out a single-factor adjustment test of boiler-related parameters, wherein the test comprises air distribution mode, opening degree of perimeter air, primary air velocity, operation oxygen content, and sulfur content in coal; the single-factor adjustment test measures the water wall reducing atmosphere, the boiler thermal efficiency, and the NOx concentration at the denitration inlet according to the adjustment of the boiler-related parameters, and statistics of the boiler steam temperature and wall temperature is carried out;S5, determining a degree of an influence of different parameters on water wall reducing atmosphere, boiler thermal efficiency, and NOx concentration at a denitration inlet; according to the single-factor adjustment test in step S4, comparing the degrees of the influence of the respective boiler-related parameters on the water wall reducing atmosphere, the boiler thermal efficiency, and the NOx concentration at the denitration inlet, and determining priorities of the respective related parameters in an optimization process;S6, carrying out an optimization test of ammonia spraying of a denitration system; under different load operating conditions, according to NOx concentration distribution at an outlet section of an SCR reactor, adjusting ammonia flows of branch pipes of each ammonia spraying grid, to cause local ammonia spraying amount to match the NOx concentration distribution;S7, carrying out a maximum safe denitration efficiency test to determine a maximum value of NOx concentration at the inlet that the denitration system can withstand; finding out a maximum safe denitration efficiency corresponding to the high load through test, and under the condition that the ammonia escape does not exceed standard, determining the maximum value of NOx concentration at the denitration inlet that the denitration system can withstand;S8, taking the maximum value of NOx concentration at the denitration inlet that the denitration system can withstand as a balance point of the NOx concentration at the denitration inlet, to determine the balance point between the water wall reducing atmosphere of the boiler and the boiler thermal efficiency, and according to the determined priorities of the boiler-related parameters in step S5, determining the optimized operation mode of the boiler.
Priority Claims (1)
Number Date Country Kind
202110267372.0 Mar 2021 CN national
CROSS-REFERENCE TO RELATED APPLICATIONS

This application claims priority to PCT Application No. PCT/CN2021/115258, having a filing date of Aug. 30, 2021, which claims priority to CN Application No. 202110267372.0, having a filing date of Mar. 12, 2021, the entire contents both of which are hereby incorporated by reference.

PCT Information
Filing Document Filing Date Country Kind
PCT/CN2021/115258 8/30/2021 WO