The invention relates to processes for cleaning or removing residues from the interior surfaces of a vacuum chamber used for fabricating electronic devices. More specifically, the invention relates to a method for the recovery of ash rate in such vacuum chambers following metal etching, in particular tungsten etching.
Processes for fabricating electronic devices containing semiconductors generally include steps in which layers or features of material are deposited or patterned (i.e., etched) within a vacuum chamber, generally called a semiconductor process chamber. The chemical by-products and unused reagents of such deposition or etch processes are mostly exhausted from the chamber by an exhaust pump, but some residue unavoidably deposits on the chamber wall and on other surfaces within the chamber. Such residue must be cleaned or removed periodically in order to maintain consistent process conditions and to prevent the residue from flaking off and contaminating the electronic device being fabricated.
A conventional method of cleaning residue from the interior surfaces of the chamber is to supply to the chamber interior a gas mixture containing radicals produced by plasma decomposition. EP-A-1 138 802 discloses a fluorine process for cleaning a semiconductor process chamber. Molecular fluorine gas (F2) is used as the principal precursor reagent.
In DRAM manufacture, the use of fluorine containing chemistries for cleaning polymers in contact Vias using suitably equipped resist strip chambers is common practice.
One such application is the polymer clean process in the so called Contact 1 Vias with exposed Metal 0 (bitline) Tungsten at the bottom of the subject contacts. It has been recently discovered that performing such a clean on the Novellus Gamma apparatus (manufactured by Novellus Systems, Inc.) using a fluorine based chemistry leads to the cumulative poisoning of the process chamber resulting in a significant drop in ash rate as well as the loss of ash rate uniformity. An investigation of this phenomenon on other competing resist strip systems such as the Mattson Aspen and the Ulvac Enviro revealed that the observed ash rate depression is also observed on those chambers as well.
Ash rate of the Novellus Gamma chamber following this poisoning cannot be recovered by known plasma clean methods in a manufacturable time frame. Also, the multi (radio frequency) RF station design of the Novellus Gamma chamber and the gas box design where the availability of the gas chemistries for overcoming the problem being restricted to the last two RF stations in the process chamber complicates and extends the ash rate recovery process.
The Novellus Gamma tool design of Novellus Systems, Inc. supports the sequential processing of up to six wafers in a common process chamber and is generally used for the purposes of resist, clean and “light” metal etch applications. The process chamber is in general plumbed with four process gases: O2, N2, N2/H2 and CF4. These are the standard gases used by most vendors that manufacture chambers for the purposes of resist strip and residue clean.
In order to support the requirements of the normal ash process, clean gases, N2/H2 and CF4 are plumbed in such a way that preferential flow of these gases are directed towards the last two stations in the process chamber. This approach of resist strip capability on the preliminary stations followed by the option to subsequently perform reduction of defects using the clean gases works well for traditional strip application. In contrast, the competitors use a process chamber with the capability of processing one or two wafers at a time. The sequence of resist strip and wafer defect cleaning is achieved by sequentially changing the process chemistry being supplied to the chamber.
The present invention discloses a manufacturable in situ chamber conditioning method that eliminates the impact of metal etch on chamber ash rate and uniformity. The present invention therefore provides a solution to ash rate excursion following metal etch.
The present invention relates to a manufacturable ash rate recovery method following metal etch. The present invention addresses the above problems by providing a process for removing residue from one or more surfaces of chamber components exposed to the interior of a semiconductor process chamber, comprising:
The process gas mixture comprises in volume % preferably from 2 to 10%, more preferably from 3 to 6 and most preferred from 3 to 5% of hydrogen and from 98 to 90%, more preferably from 97 to 94% and most preferred from 97 to 95% of nitrogen.
In a preferred method according to the present invention, the recovery method is automated to minimize tool down time, to avoid the risk of cross contamination as well as maintain process stability.
The ash rate recovery method of the present invention is not limited to the Novellus Gamma platform, but can be also applied to other ash tool platforms.
In a preferred embodiment of the present invention, the gas mixture contains in addition to nitrogen (N2) and hydrogen (H2) in volume % preferably from 2 to 10%, more preferably from 3 to 6 and most preferred from 3 to 5% of hydrogen and from 98 to 90%, more preferably from 97 to 94% and most preferred from 97 to 95% of nitrogen as a further component CF4.
In an even more preferred embodiment, the gas mixture contains furthermore O2. It has been found that the addition of O2 can avoid the formation of polyfluoroethylene type polymers generated in the plasma when hydrogen gas is used in combination with CF4.
The method of the present invention has a number of advantages. For example, it does not cause ash rate or uniformity degradation when used following standard ash process without metal etch.
Moreover, with the removal of metal etch residues from the process chamber, the risk of cross-contamination between wafers and lots is minimized.
The present invention is further illustrated by way of examples which are not meant to be limiting the scope of the invention.
Ash rate depression following W, AlCu and TiN etch could be recovered using a gas mixture of 2000 sccm O2, 8000 sccm N2/H2 and 40 sccm CF4 at a process pressure of 1100 mtorr and an RF power of 2000 W. The processing time for such a recovery following metal etch was 60 seconds.
The risk of Tungsten contaminant transfer from a contaminated process chamber to wafers being processed was eliminated by conditioning the process chamber immediately following Tungsten etch. The conditioning method was to expose the process chamber for 60 seconds to a gas mixture containing 2000 sccm O2, 8000 sccm N2/H2 and 40 sccm CF4 at a process pressure of 1100 mtorr and an RF power of 2000 W.
The chamber was then conditioned using the proposed technique and a new monitor wafer was processed through the tool to recheck the level of Tungsten contamination. An ICP-MS evaluation indicated a Tungsten contamination level of 0.126E10 atoms/cm2. An acceptable metal contamination level specified for semiconductor equipment is typically 10E10 atoms/cm2.
The present invention allows to remove the blue WO2 coating along the chamber walls and top chamber cover plate which is visible in a poisoned chamber. The WO2 is presumably formed by the reaction of WF5 or WFx with oxygen radical which firstly gives rise to a white residue visible in a poisoned chamber which is believed to be WOF4. This reaction is believed to be the main scavenging reaction to suppress ash rate. WOF4 may undergo further transformation to WO2F2 and WO3 either through hydrolysis or through further scavenging of oxygen radicals from the plasma.
A design of experiment was performed to evaluate the process window for chamber ash rate and uniformity recovery by intentionally contaminating the process chamber with Tungsten. During the chamber ash rate recovery, O2, Forming gas, CF4 flows were varied and so was the applied RF plasma power. Results from this experiment are tabulated below. A percentage recovery higher than ˜95% indicates complete recovery of the indicated parameter since small variations in parameters from one run to the next is to be expected.
The chamber pressure was in range of from 0.5 to 2 Torr, preferred of from 0.5 to 2 Torr, most preferred of from 0.8 to 1.5 Torr. In a specific embodiment of the invention, the pressure was 1.1 Torr.
The process used in experiment 2 above was further evaluated by processing 25 Tungsten wafers at a time to contaminate the process chamber and then running the 60 second recovery process. The process of running the 25 Tungsten wafers and the recovery was repeated 4 times to test the process stability. The stability of the ash rate and uniformity is evident from the graph of
In order to demonstrate that the ash rate recovery process does not degrade the chamber ash rate and uniformity performance when applied on chambers not exposed to Tungsten contamination, the recovery process was run following the processing of bare Si wafers. Following the completion of the 60 second recovery process, the chamber ash rate and uniformity was qualified. Results from a series of back-to-back experiments to demonstrate stability is shown in the graph of