1. Field of the Invention
The present invention relates to an operation method of a nuclear power plant and to a nuclear power plant. More particularly, the present invention relates to an operation method of a nuclear power plant and to a nuclear power plant, which are suitable for an uprate of normal operation power output of a nuclear power plant.
2. Description of the Related Art
In a newly constructed nuclear power plant, electric power has hitherto been uprated, for example, by improving the fuel makeup or the shape and makeup of a fuel assembly so as to increase the flow rate of main steam at a core outlet.
Such related art is disclosed in Patent Document 1 (JP,A 9-264983).
When the above-mentioned related art is applied to the existing nuclear power plant, the rate of core flow passing through a reactor core is substantially the same as that before the power uprate, while thermal power of the core is increased. In a boiling water reactor (BWR), therefore, an average void rate (proportion of steam with respect to the channel volume) in the core is increased. Accordingly, the flow speed of a coolant is increased and so is a pressure loss in the core. Also, with an increase in the amount of steam generated in the core, a pressure loss in a water-steam two-phase flow section is increased and a margin of core safety tends to reduce. Further, an increase of the average void rate in the core increases an amount of steam condensed in the so-called pressure transient state where pressure rises, for example, when a generator load is cut off, thus resulting in a larger amount of decrease of the average void rate in the core. Generally, the boiling water reactor has a negative void feedback coefficient so that the reactor power reduces as the void rate increases. In the pressure transient state, however, the average void rate in the core is reduced and the reactor power is increased. Thus, the related art has a possibility that, after the power uprate, the amount of decrease of the average void rate in the core is increased in the pressure transient state and a design margin for pressure transient events is reduced.
Meanwhile, the flow rate of main steam is increased substantially in proportion to an increase of the power uprate. The increased flow rate of main steam reduces design margins of almost all equipment, such as feedwater equipment including feedwater piping, a feedwater heater, a feedwater pump, etc., pressure vessel internals including a dryer, etc., a main steam line, a high pressure turbine, a low pressure turbine, and a condenser. In a usual nuclear power plant employing a boiling water reactor, the high pressure turbine is one of the equipment with a possibility that the design margin is first lost with the increase in the flow rate of main steam. Also, in a nuclear power system other than the boiling water reactor, a similar problem arises in a plant where the design margin for the high pressure turbine is relatively small. Accordingly, when the related art is applied to the existing nuclear power plant, large-scaled improvement and replacement of plant equipment are required. The increase in the flow rate of main steam can be suppressed by lowering the feedwater temperature. However, such a solution is not realistic for the reason that, if the flow rate of steam extracted for heating the feedwater is simply reduced as a whole, thermal efficiency is noticeably deteriorated and the electric power is not increased in proportion to the core thermal power output.
An object of the present invention is to provide an operation method of a nuclear power plant, which can uprate plant power without greatly modifying the construction of plant equipment, while keeping a core's pressure loss characteristic, a safety margin, and a design margin in the transient state substantially the same as those before the power uprate.
To achieve the above object, according to one aspect of the present invention, assuming that one operation cycle is defined as a period from a time at which a nuclear power plant starts operation to a time at which the nuclear power plant stops the operation for fuel exchange, second reactor thermal power in a second operation cycle of a nuclear reactor is uprated from first reactor thermal power in a first operation cycle preceding the second operation cycle at least one operation cycle, and a proportion of steam extracted from a steam system and introduced to a feedwater heater, which is in particular extracted from an intermediate point of a high pressure turbine and an outlet thereof (practically, some point in a section ranging from the outlet of the high pressure turbine to an inlet of one of a moisture separator, a moisture separator and heater, and a moisture separator and reheater), with respect to a flow rate of main steam is reduced in the second operation cycle from a proportion in the first operation cycle such that temperature of feedwater discharged from the feedwater heater lowers in the range of 1° C. to 40° C. in the second operation cycle.
To achieve the above object, according to another aspect of the present invention, second reactor thermal power in a second operation cycle of a nuclear reactor is uprated from first reactor thermal power in a first operation cycle preceding the second operation cycle at least one operation cycle, and a mass flow rate of steam extracted from a steam system and introduced to a feedwater heater, which is in particular extracted from an intermediate point and an outlet of a high pressure turbine, is reduced in the second operation cycle from a mass flow rate of steam extracted in the first operation cycle such that temperature of feedwater discharged from the feedwater heater lowers in the range of 1° C. to 40° C. in the second operation cycle.
To achieve the above object, according to still another aspect of the present invention, second reactor thermal power in a second operation cycle of a nuclear reactor is uprated from first reactor thermal power in a first operation cycle preceding the second operation cycle at least one operation cycle, and a temperature rise in one of a plurality of feedwater heaters, particularly a high pressure feedwater heater installed downstream of a main feedwater pump, is reduced in the second operation cycle such that temperature of feedwater discharged from the feedwater heater lowers in the range of 1° C. to 40° C. in the second operation cycle.
To achieve the above object, according to still another aspect of the present invention, second reactor thermal power in a second operation cycle of a nuclear reactor is uprated from first reactor thermal power in a first operation cycle preceding the second operation cycle at least one operation cycle, and at least one of extraction lines for extracting steam from a steam system and introducing the extracted steam to a feedwater heater, which is in particular extended from an intermediate point and an outlet of a high pressure turbine, is shut off such that temperature of feedwater discharged from the feedwater heater lowers in the range of 1° C. to 40° C. in the second operation cycle.
To achieve the above object, according to another aspect of the present invention, second reactor thermal power (Q2) in a second operation cycle of a nuclear reactor is uprated A % from first reactor thermal power (Q1) in a first operation cycle preceding the second operation cycle at least one operation cycle, and a proportion of steam extracted from a steam system and introduced to a feedwater heater, which is in particular extracted from an intermediate point of a high pressure turbine and an outlet thereof (practically, some point in a section ranging from the outlet of the high pressure turbine to an inlet of one of a moisture separator, a moisture separator and heater, and a moisture separator and reheater), with respect to a flow rate of main steam in the second operation cycle is kept equivalent to or reduced from a proportion in the first operation cycle such that the following formulae are satisfied;
0<A≦5, and
T2≦T1−7.7×(Q2−Q1)/(4.5×W)
where temperature of the feedwater discharged from the feedwater heater in the first operation cycle is T1 (° C.), temperature of the feedwater discharged from the feedwater heater in the second operation cycle is T2 (° C.), and a core flow rate of the feedwater flowing into the nuclear reactor in the second operation cycle is W (kg/s).
To achieve the above object, according to another aspect of the present invention, second reactor thermal power (Q2) in a second operation cycle of a nuclear reactor is uprated A % from first reactor thermal power (Q1) in a first operation cycle preceding the second operation cycle at least one operation cycle, and a proportion of steam extracted from a steam system and introduced to a feedwater heater, which is in particular extracted from an intermediate point of a high pressure turbine and an outlet thereof (practically, some point in a section ranging from the outlet of the high pressure turbine to an inlet of one of a moisture separator, a moisture separator and heater, and a moisture separator and reheater), with respect to a flow rate of main steam in the second operation cycle is kept equivalent to or reduced from a proportion in the first operation cycle such that the following formulae are satisfied;
5<A≦10, and
T1−40≦T2≦T1−7.7×(Q2×(A+95)/100−Q1)/(4.5×W)
where temperature of the feedwater discharged from the feedwater heater in the first operation cycle is T1 (° C.), temperature of the feedwater discharged from the feedwater heater in the second operation cycle is T2 (° C.), and a core flow rate of the feedwater flowing into the nuclear reactor in the second operation cycle is W (kg/s).
To achieve the above object, according to another aspect of the present invention, second reactor thermal power (Q2) in a second operation cycle of a nuclear reactor is uprated A % from first reactor thermal power (Q1) in a first operation cycle preceding the second operation cycle at least one operation cycle, and a proportion of steam extracted from a steam system and introduced to a feedwater heater, which is in particular extracted from an intermediate point of a high pressure turbine and an outlet thereof (practically, some point in a section ranging from the outlet of the high pressure turbine to an inlet of one of a moisture separator, a moisture separator and heater, and a moisture separator and reheater), with respect to a flow rate of main steam in the second operation cycle is kept equivalent to or reduced from a proportion in the first operation cycle such that the following formulae are satisfied;
10<A<30, and
T2≦T1−7.7×(Q2×(A+90)/100−Q1)/(4.5×W)
where temperature of the feedwater discharged from the feedwater heater in the first operation cycle is T1 (° C.), temperature of the feedwater discharged from the feedwater heater in the second operation cycle is T2 (° C.), and a core flow rate of the feedwater flowing into the nuclear reactor in the second operation cycle is W (kg/s).
To achieve the above object, according to still another aspect of the present invention, a nuclear power plant comprises an extracted flow control valve disposed in at least one extraction line; a temperature sensor disposed in a feedwater system at a point between adjacent two of a plurality of feedwater heaters disposed in the feedwater system or at a point downstream of one of the plurality of feedwater heaters which is positioned most downstream; and an extracted flow controller for outputting an opening request command for the extracted flow control valve based on a measured value from the temperature sensor and a set value of feedwater temperature, wherein the nuclear power plant is operated such that second nuclear thermal power in a second operation cycle of the nuclear reactor is uprated from first nuclear thermal power in a first operation cycle before the second operation cycle, and second feedwater temperature in the second operation cycle is made lower than first feedwater temperature in the first operation cycle.
Since the feedwater temperature can be adjusted to a set value through control of the opening of the extracted flow control valve, it is possible to suppress variations in the amount of power generated during the power uprate operation of the nuclear power plant.
To achieve the above object, according to still another aspect of the present invention, a nuclear power plant comprises an extracted flow control valve and an extraction flow rate measuring meter disposed in at least one extraction line; and an extracted flow controller for outputting an opening request command for the extracted flow control valve based on a measured value from the extraction flow rate measuring meter and a set value of a flow rate of the extracted steam, wherein the nuclear power plant is operated such that second nuclear thermal power in a second operation cycle of the nuclear reactor is uprated from first nuclear thermal power in a first operation cycle before the second operation cycle, and second feedwater temperature in the second operation cycle is made lower than first feedwater temperature in the first operation cycle.
To achieve the above object, according to still another aspect of the present invention, a nuclear power plant comprises an extracted flow control valve disposed in at least one extraction line; at least one main steam flow rate measuring meter disposed in a steam system between the nuclear reactor and the high pressure turbine; and an extracted flow controller for outputting an opening request command for the extracted flow control valve based on a measured value from the main steam flow rate measuring meter and a set value of a flow rate of the main steam, wherein the nuclear power plant is operated such that second nuclear thermal power in a second operation cycle of the nuclear reactor is uprated from first nuclear thermal power in a first operation cycle before the second operation cycle, and second feedwater temperature in the second operation cycle is made lower than first feedwater temperature in the first operation cycle.
According to the present invention, in trying to uprate power of the existing nuclear power plant, the power uprate of the nuclear power plant can be realized without greatly modifying the construction of the nuclear power plant, while keeping a core's pressure loss characteristic, a safety margin, a thermal margin, and a design margin in the transient state substantially the same as those before the power uprate.
A first embodiment represents the case where the present invention is applied to a boiling water reactor system as one of nuclear power plants.
The overall construction of the boiling water reactor system according to this embodiment will be first described with reference to
In
Extraction lines 25, 26, 27 and 28 for extracting steam from the steam system 22 and introducing the extracted steam to the high pressure feedwater heater 9 and the low pressure feedwater heater 7 are disposed between the steam system 22 and corresponding one of the high pressure feedwater heater 9 and the low pressure feedwater heater 7. The extraction line 25 extracts steam from an intermediate point of the high pressure turbine 3 and introduces the steam to the high pressure feedwater heater 9. The extraction line 26 extracts steam from an outlet of the high pressure turbine 3 (actually some point downstream of the outlet of the high pressure turbine 3 and upstream of an inlet of the moisture separator 4) and introduces the steam to the high pressure feedwater heater 9. The extraction line 27 extracts steam from an intermediate point of the moisture separator 4 and introduces the steam to the low pressure feedwater heater 7. The extraction line 28 extracts steam from an intermediate point of the low pressure turbine 5 and introduces the steam to the low pressure feedwater heater 7. An extraction line flow adjusting valve 10, i.e., extracted steam amount adjusting means for adjusting an extracted steam amount introduced from the intermediate point of the high pressure turbine 3 to the high pressure feedwater heater 9, is disposed in the extraction line 25.
The operation method of the thus-constructed nuclear power plant according to this embodiment will be described below. In
In the heat balances shown in
Looking from another aspect, according to the operation method of this embodiment, the mass flow rate (G=3+10=13) of steam extracted from the high pressure steam system 22A is reduced (G=19→13) in the second operation cycle (
The operation method of this embodiment will be described in more detail below.
Of operation cycles shown in
When the reactor thermal power is uprated, the flow rate of the feedwater has to be increased or the enthalpy difference of a coolant between the inlet and the outlet of the reactor pressure vessel has to be increased in order to remove heat that has increased in amount corresponding to the power uprate. The known power uprating method employs the former manner; namely it increases the flow rate of the feedwater in proportion to the reactor thermal power. An example of heat balance according to the known power uprating method is shown in
In a plant where the flow rate of steam extracted from the intermediate point of the high pressure turbine 3 or the outlet of the high pressure turbine 3 is originally small, the flow rate of steam extracted from the low pressure turbine 5 has to be also reduced in order to sufficiently lower the feedwater temperature. Even when the present invention is applied to such a plant, a certain effect can be obtained by reducing the flow rate of steam extracted from the intermediate point of the high pressure turbine 3 or the outlet of the high pressure turbine 3 to a larger extent. With this embodiment, in spite of increasing the reactor thermal power by 5% as compared with the N-th operation cycle, the flow rate of the main steam can be kept the same as that in the N-th operation cycle. Because this embodiment is described in connection with the ideal power uprating method, the flow rate of the main steam is the same in both the N-th operation cycle and the (N+1)-th operation cycle. However, the flow rate of the main steam is not always required to be the same in those operation cycles, and the flow rate of the main steam may be increased within the range of a design margin of the equipment including the high pressure turbine 3.
When there are a plurality of extraction points usable to reduce the flow rate of the extracted steam, i.e., when there are a plurality of extraction points midway the high pressure turbine 3 or at the outlet of the high pressure turbine 3, a maximum effect can be obtained by selecting the most upstream extraction point. In such a case, while the extraction line flow adjusting valve 10 for controlling the flow rate of the extracted steam may be disposed to reduce the flow rate of the extracted steam, one or more of the extraction lines may be completely closed as an alternative manner. To close the extraction line, a shut-off valve is disposed midway the extraction line, or the extraction line is plugged. When the extraction line is completely closed, equipment for controlling the flow rate of the extracted steam is not required and the operation control is simplified. Whether to control the flow rate of the extracted steam or completely close the extraction line depends on the heat balance and the extent of power uprate in the plant. (In the case where the flow rate of the extracted steam per extraction line is too large, the feedwater temperature is excessively lowered if the extraction line is completely closed. Therefore, the flow rate of the extracted steam is adjusted in that case.)
According to this embodiment, even when the reactor thermal power is uprated to increase the amount of power generated in the nuclear power plant, increases of both the flow rate of the feedwater and the flow rate of the main steam can be suppressed, whereby an increase of burdens imposed on the feedwater line 24, the main steam line 2, and the pressure vessel internals can be suppressed. As compared with the case of simply reducing the flow rate of the extracted steam as a whole, it is possible to suppress decrease of the thermal efficiency and to obtain larger electric power. Further, although the high pressure turbine 3 must be usually replaced when power is uprated to a large extent by the known power uprating method, this embodiment can provide a wider power uprate range available without replacing the high pressure turbine 3 than that provided by the known method.
With the operation method of this embodiment, the feedwater temperature is lowered. The lowering of the feedwater temperature lowers the coolant temperature at the core inlet and increase the thermal margin of the core (corresponding to MCPR (Minimum Critical Power Ratio) in BWR), thus resulting in an advantage of ensuring higher safety than that obtained with the known power uprating method. The conventional power uprate increases the core pressure loss and reduces the safety margin if the same fuels are used. In contrast, the power uprating method of the present invention lowers the coolant temperature at the core inlet and reduces the void rate and the absolute value of the void coefficient in the core. Therefore, the core pressure loss is reduced and a reduction of the safety margin of the core is suppressed. Further, the design margin for the pressure rising transient state is increased with the reduction of the void rate and the absolute value of the void coefficient in the core.
Thus, the lowering of the feedwater temperature is effective in suppressing the deterioration of core characteristics and the reduction of the design margin in the boiling water reactor during the power update operation. Generally, because feedwater temperature control is not especially performed in the boiling water reactor, the feedwater temperature may change to the extent of smaller than 1° C. even in the same boiling water reactor and at the same core thermal power due to change of heat balance in the entire plant, in particular temperature change of the coolant (seawater in many cases) that is used to condense the steam by the condenser 6 shown in
The reduction of the core pressure loss means that an increase of loads imposed on the jet pump and the recirculation pump, which are used for recirculation of the coolant, due to the power uprate can also be suppressed. Further, since the amount of increase in quantity of steam generated in the core is comparatively smaller than that of the thermal power, an influence upon the carry under caused by entrainment with the recirculation water can also be kept small and the flow window can be easily ensured even in the case of large power uprate.
Table 1, given below, shows the relationships among the reactor thermal power, the flow rate of the main steam, the flow rate of the extracted steam, and the enthalpy of the feedwater when the power uprating method of this embodiment is applied to the cases of uprating the power at various rates. Each value of the reactor thermal power and the flow rate of the main steam represents a ratio relative to that at 100% of the reactor thermal power, and a value of the flow rate of the extracted steam represents a ratio relative to the flow rate of the main steam at 100% of the reactor thermal power. As seen from Table 1, the power uprating method of this embodiment can be applied over a wide range including even the case where the reactor thermal power is uprated to 110%. The reason why Table 1 shows only the power uprate up to 110% is that the power uprate in excess of 110% requires replacement of the moisture separator 4. If the replacement of the moisture separator 4 is allowed or a combination with, e.g., an increase of the core pressure and/or with employment of a moisture separator and reheater is considered, the power uprating method of this embodiment can be applied over a wider range of power uprate.
In the boiling water reactor, uprate of the reactor thermal power up to about 102% is generally feasible just by increasing the measurement accuracy of a feedwater flowmeter, etc. Therefore, the present invention is more effective when applied to the case of uprating the reactor thermal power in excess of 102%. Further, at the power uprate up to about 105% of the reactor thermal power, substantial change of system equipment, e.g., replacement of the high pressure turbine 3, is not required in general. The effect of this embodiment is especially noticeable when applied to the uprate of the reactor thermal power in excess of 105% because the replacement of the high pressure turbine 3 is not required even in that case.
In view of the above-mentioned fact that substantial change of system equipment, e.g., replacement of the high pressure turbine 3, is not required in general at the ordinary power uprate up to about 105% of the reactor thermal power, an application method of this embodiment may be changed between the case of uprating the reactor thermal power at a rate of not larger than 5% and the case of uprating the reactor thermal power at a rate of larger than 5%. More specifically, because the replacement of the high pressure turbine 3 is not required when the increase rate of the reactor thermal power is not larger than 5%, it is primarily intended to keep the above-mentioned core characteristic (core average void rate) the same as that before the power uprate. Assuming that the reactor thermal power before the power uprate is Q1 (kW), the reactor thermal power after the power uprate is Q2 (kW), and the increase rate of the power uprate is A (%), the power uprate of not larger than 5% is expressed by A≦5. Also, on an assumption that the core flow rate after the power uprate is W (kg/s), the specific heat at constant pressure at about 200° C. under 7 MPa, i.e., the operating pressure in a typical boiling water reactor, is about 4.5 (kJ/kg·K), and a proportion of the flow rate of the feedwater with respect to the core flow rate in the typical boiling water reactor is about 13%, the condition for keeping the core average void rate the same as that before the power uprate is given as follows.
Change in thermal value of the feedwater per 1° C. of the feedwater temperature is expressed by:
W (kg/s)×13(%)/100(%)×4.5 (kJ/kg·K)=W×13/100×4.5 (kW/K)
Assuming here that the feedwater temperature before the power uprate is T1 and the feedwater temperature after the power uprate is T2, the feedwater temperature T2 required to reduce the thermal value of the feedwater, which is equivalent to the thermal value (Q2−Q1) (kW) corresponding to the power uprate, is determined by the following equation:
Q2−Q1=W×13/100×4.5×(T1−T2)
In order to hold the core characteristics equivalent to or better than those before the power uprate, the feedwater thermal value is just required to be reduced by an amount of not smaller than the thermal value increased with the power uprate. The condition to meet such a requirement is expressed by:
Q2−Q1≦W×13/100×4.5×(T1−T2)
This formula is rewritten into:
T2≦T1−7.7×(Q2−Q1)/(4.5×W)
Stated another way, by setting the feedwater temperature so as to satisfy the above formula in the case of the power uprate of not larger than 5%, the core characteristics, such as the thermal margin, the pressure loss characteristic, the safety margin, and the design margin in the transient state of the core, can be basically held equivalent to or better than those before the power uprate. Further, since the flow rate of the main steam is kept equivalent to or reduced from that before the power uprate, the design margin of the main steam system, including the high pressure turbine and the dryer, can also be held equivalent to or better than those before the power uprate.
A description is made of the feedwater temperature when the nuclear thermal power is uprated at a rate of larger than 5%, but not larger than 10%. When the nuclear thermal power is uprated at a rate of larger than 5% by the known power uprating method, the flow rate of the main steam is also increased in excess of 5%, thus generally resulting in that the design margin of equipment, e.g., the high pressure turbine, is exceeded. Therefore, such equipment has to be replaced. In that case, by lowering the feedwater temperature as in this embodiment, the increase in the flow rate of the main steam can be held not larger than 5%.
Assuming here that the increase in the flow rate of the main steam up to 5% is allowed, a reduction of the feedwater thermal value required when the power uprate is increased at A (%) corresponds to the power increase of (A−5) % and is expressed by:
Q2×(A−5+100)/100−Q1=Q2×(A+95/100)−Q1
On the assumption that the feedwater temperature before the power uprate is T1 and the feedwater temperature after the power uprate is T2, the above thermal value can be offset when T1 and T2 satisfy the following formula:
Q2×(A+95/100)−Q1=W×13/100×4.5×(T1−T2)
Thus, the increase in the flow rate of the main steam can be held not larger than 5% by satisfying:
Q2×(A+95/100)−Q1≦W×13/100×4.5×(T1−T2)
With rewrite of this formula, T2 is expressed by:
T2≦T1−7.7×(Q2×(A+95)/100)−Q1)/(4.5×W)
In the case of the power uprate being larger than 5%, but not larger than 10%, therefore, if the feedwater temperature T2 satisfies the above formula, the power uprate can be realized within the range of the design margin of the high pressure turbine, etc. and the replacement of such equipment is not required. Further, the design margins of the high pressure turbine and the core can be held equivalent to or larger than those resulting at the power uprate of 5% by the known method.
At the power uprate in excess of 10%, it is generally required in the boiling water reactor to replace, e.g., the moisture separator in addition to the high pressure turbine, etc. This problem can be overcome by lowering the feedwater temperature in a similar manner to hold the increase in the flow rate of the main steam to be not larger than 10% so that the replacement of the moisture separator is not required. The condition of meeting such a requirement in this case is given as follows for the rate A (%) of the power uprate based on the same concept as that when the power uprate is larger than 5%, but not larger than 10%:
Q2×(A−10+100)/100−Q1≦W×13/100×4.5×(T1−T2)
With rewrite of this formula, T2 is expressed by:
T2≦T1−7.7×(Q2×(A+90)/100−01)/(4.5×W)
This indicates an extent of lowering of the feedwater temperature within which the replacement of the moisture separator is not required at the power uprate of larger than 10%. In that case, the design margins of the high pressure turbine and the core can also be held equivalent to or larger than those resulting at the power uprate of 10% by the known method.
At any of the power uprate of not larger than 5%, the power uprate of larger than 5%, but not larger than 10%, and the power uprate of larger than 10%, the extent of lowering of the feedwater temperature in excess of 40° C. is undesired in practice from the viewpoint of thermal fatigue. Also, as the power uprate increases, the thermal margin of the core is reduced. It can be generally said that the thermal margin of the core is bearable for the power uprate up to about 20% by employing new fuel. Another conceivable solution is to improve, e.g., a pump for increasing the core flow rate. Even in consideration of such an improvement as well, the power uprate at a rate of about 30% is regarded to be a limit from the viewpoint of the core characteristics. Further, looking at the equipment side, the power uprate over 30% is also not desired in practice because such large power uprate exceeds the design limits of the low pressure turbine and the condenser, which are more expensive than the high pressure turbine, and hence requires replacement of those other units of equipment.
According to this embodiment, for the power uprate of not larger than 5%, the power uprate can be realized while holding the design margins of the high pressure turbine and the core equivalent to or larger than those before the power uprate. For the power uprate of larger than 5%, but not larger than 10%, the power uprate can be realized up to 10% while holding the design margins of the high pressure turbine and the core equivalent to or larger than those resulting at the power uprate of 5% by the known method. For the power uprate of larger than 10%, the power uprate can be realized in excess of 10% with no need of replacing the moisture separator, etc. while holding the design margins of the moisture separator and the core equivalent to or larger than those resulting at the power uprate of 10% by the known method.
The present invention can be modified in various ways without being restricted to the above-described embodiment. For example, in the boiling water reactor system, a moisture separator and heater or a moisture separator and reheater 11, shown in
While the above embodiment is described as applying the present invention to the boiling water reactor power plant, the present invention is applicable to a pressurized water reactor system as well.
Another embodiment of the present invention in which the invention is applied to the boiling water reactor power plant as one of nuclear power plants will be described below with reference to
As in the first embodiment, he boiling water reactor power plant of this embodiment comprises a reactor pressure vessel 1, a main steam line 2, a high pressure turbine 3 and a low pressure turbine 5 connected to the main steam line 2 in series, and a moisture separator 4 (or a moisture separator and heater) disposed in the main steam line 2 between the high pressure turbine 3 and the low pressure turbine 5. A low pressure feedwater heater 7, a feedwater pump 8, and a high pressure feedwater heater 9 are installed in a feedwater system 23 downstream of a condenser 6.
When the reactor thermal power is uprated, the flow rate of the feedwater has to be increased or the enthalpy difference of the coolant between the inlet and the outlet of the reactor pressure vessel 1 has to be increased in order to remove heat that has increased in amount corresponding to the power uprate. The known power uprating method employs the former manner; namely it increases the flow rate of the feedwater in proportion to the reactor thermal power. On the other hand, as a new power uprating method, there is also proposed a method of suppressing increases of both the flow rate of the main steam and the flow rate of the feedwater in the power uprate operation based on the latter manner by intentionally reducing the coolant enthalpy (temperature) at the inlet of the reactor pressure vessel, to thereby increase the enthalpy difference between the inlet and the outlet of the reactor pressure vessel. This embodiment is adapted for such a new power uprating method and requires additional equipment for widening a feedwater temperature controllable range so that the feedwater temperature is lowered to a value beyond the range estimated in the stage of plant construction.
The necessity of widening the feedwater temperature controllable range toward the lower temperature side in turn requires the flow rate of steam extracted for heating the feedwater to be reduced in comparison with that before the power uprate. The steam extracted from the high pressure turbine 3 for heating the feedwater is introduced to the high pressure feedwater heater 9 via extraction lines 25 and 26. Also, the steam extracted from the low pressure turbine 5 is sent to the low pressure feedwater heater 7 via an extraction line 28. An extracted flow control valve 38 is disposed in the extraction line 25 to adjust the flow rate of the extracted steam. In the boiling water reactor power plant of this embodiment, a plurality of main extraction lines are installed downstream of the inlet of the high pressure turbine and upstream of the outlet of the low pressure turbine.
In the boiling water reactor power plant of this embodiment to which the above-mentioned new power uprating method is applied, it is important that the feedwater temperature be surely lowered to a preset value. For that reason, a feedwater temperature sensor 39 is disposed in the feedwater system 23 downstream of the high pressure feedwater heater 9 that is located most downstream in the feedwater system 23. The feedwater temperature sensor 39 measures the temperature of the feedwater discharged from the high pressure feedwater heater 9 and outputs a feedwater temperature measured value signal 41. An extracted flow controller 40 controls the opening of the extracted flow control valve 38 to adjust the flow rate of the extracted steam. The feedwater temperature sensor 39 is disposed in the feedwater system 23 downstream of the high pressure feedwater heater 9, to which the extracted steam is supplied at the adjusted flow rate, and upstream of the inlet of the reactor pressure vessel 1. Alternatively, the feedwater temperature sensor 39 may be disposed between the high pressure feedwater heater 9 and another suitable feedwater heater installed downstream of the former.
One example of control logic executed by the extracted flow controller 40 in the second embodiment will be described below with reference to
According to this embodiment, since the feedwater temperature can be adjusted to the set value through control of the opening of the extracted flow control valve 38, it is possible to suppress variations in the amount of power generated during the power uprate operation of the nuclear power plant.
Also, according to this embodiment, since the feedwater temperature can be always held at the set value, it is possible to suppress the increases of both the flow rate of the main steam and the flow rate of the feedwater by lowering the feedwater temperature in the power uprate operation of the reactor. Further, since the feedwater temperature can be adjusted in real time, even in the case of changing the thermal power of the nuclear power plant, the operation method of this embodiment is adaptable for the load following operation of the nuclear power plant by modifying the set value of the feedwater temperature depending on the change of the thermal power, while the flow rate of the main steam and the flow rate of the feedwater are held constant.
A boiling water reactor power plant according to still another embodiment (third embodiment) of the present invention will be described below with reference to
This third embodiment differs from the second embodiment in that, instead of the feedwater temperature sensor 39, an extraction flowmeter 44 is disposed in the extraction line 25 in which the extracted flow control valve 38 is disposed. The extracted flow controller 40 receives a measured value from the extraction flowmeter 44 and a set value of the flow rate of the extracted steam. The extraction flowmeter 44 measures the flow rate of the extracted steam supplied to the high pressure feedwater heater 9. The extracted flow control valve 38 and the extraction flowmeter 44 may be disposed in the extraction line 25 irrespective of which one of them is positioned upstream of the other. When the extraction line 25 is merged midway with another extraction line (e.g., the extraction line 26), one of the extracted flow control valve 38 and the extraction flowmeter 44, which is positioned on the downstream side, may be disposed in the extraction line 25 downstream of the merging point between the two extraction lines. Also, when the extraction line 25 is branched midway, one of the extracted flow control valve 38 and the extraction flowmeter 44, which is positioned on the downstream side, may be disposed in a line after being branched. If the reactor thermal power, the flow rate of the feedwater, and the flow rate of the extracted steam are known, the feedwater temperature is uniquely decided from the heat balance of the nuclear power plant. Accordingly, measuring the flow rate of the extracted steam by the extraction flowmeter 44 disposed in the extraction line 25, as in this embodiment, is equivalent to measurement of the feedwater temperature.
In this embodiment, the extracted flow controller 40 receives an extracted flow measured value signal 45 outputted from the extraction flowmeter 44 and a set value signal 42A for the flow rate of the extracted steam. Based on the extracted flow measured value signal 45 and the extracted flow set value signal 42A, the extracted flow controller 40 outputs an opening demand signal 43 for the extracted flow control valve 38. The opening of the extracted flow control valve 38 is controlled in accordance with the opening demand signal 43. If the measured value of the flow rate of the extracted steam is smaller than the set value of the flow rate of the extracted steam, this means that the flow rate of the extracted steam is insufficient. Therefore, the extracted flow controller 40 outputs the opening demand signal 43 to increase the opening of the extracted flow control valve 38. Conversely, if the measured value of the flow rate of the extracted steam is larger than the set value, this means that the flow rate of the extracted steam is too large. Therefore, the extracted flow controller 40 outputs the opening demand signal 43 to reduce the opening of the extracted flow control valve 38. This third embodiment can also provide similar advantages to those obtainable with the second embodiment.
A boiling water reactor power plant according to still another embodiment (fourth embodiment) of the present invention will be described below with reference to
A boiling water reactor power plant according to still another embodiment (fifth embodiment) of the present invention will be described below with reference to
In this fifth embodiment, a main steam flowmeter 46 is disposed in the main steam system 2 between the reactor pressure vessel 1 and the high pressure turbine 3. If the reactor thermal power and the flow rate of the main steam are known, the feedwater temperature is uniquely decided from the heat balance of the nuclear power plant. Accordingly, measuring the flow rate of the main steam by the main steam flowmeter 46 disposed in the main steam system 22, as in this fifth embodiment, is equivalent to the measurement of the feedwater temperature in the second embodiment. The arrangement of this fifth embodiment is similar to that of the second embodiment except that the main steam flowmeter 46 is disposed instead of the feedwater temperature sensor 39 and the extracted flow controller 40 controls the extracted flow control valve 38 in accordance with the measured value from the main steam flowmeter 46.
In this embodiment, the extracted flow controller 40 receives a main-steam flow measured value signal 47 outputted from the main steam flowmeter 46 and a set value signal 48 for the flow rate of the main steam. Then, the extracted flow controller 40 produces an opening demand signal 43 based on those two signals and outputs it to the extracted flow control valve 38. If the measured value of the flow rate of the main steam is smaller than the set value of the flow rate of the main steam, this means that the feedwater temperature is too low, namely the flow rate of the extracted steam is insufficient. Therefore, the extracted flow controller 40 outputs the opening demand signal 43 to increase the opening of the extracted flow control valve 38. Conversely, if the measured value of the flow rate of the main steam is larger than the set value, this means that the feedwater temperature is too high, namely the flow rate of the extracted steam is too large. Therefore, the extracted flow controller 40 outputs the opening demand signal 43 to reduce the opening of the extracted flow control valve 38. This fifth embodiment can also provide similar advantages to those obtainable with the second embodiment.
A boiling water reactor power plant according to still another embodiment (sixth embodiment) of the present invention will be described below with reference to
Instead of the above-described arrangement, the main steam flowmeter 46 and the feedwater temperature sensor 39 may be disposed to perform the control based on the flow rate of the main steam and the control based on the feedwater temperature. Further, the main steam flowmeter 46 and the extraction flowmeter 44 may be disposed to perform the control based on the flow rate of the main steam and the control based on the flow rate of the extracted steam.
Generally, when the flow rate of the extracted steam is reduced to lower the feedwater temperature, the thermal efficiency of the plant is reduced. In order to suppress such a reduction of the thermal efficiency, it is preferable to reduce the flow rate of the steam extracted from the extraction point that is positioned as close as possible to the uppermost side. Therefore, a greater effect can be obtained by installing the extracted flow control valve 38 in the extraction line for extracting the steam from a point downstream of the inlet of the high pressure turbine and upstream of the inlet of the lower pressure turbine. While the extracted flow control valve 38 is disposed only in one extraction line in the second to sixth embodiments, the feedwater temperature cannot be sufficiently lowered in some cases by reducing the flow rate of the extracted steam through only one extraction line. In such a case, the extracted flow control valve 38 is disposed in plural extraction lines.
In the boiling water reactor power plant, as mentioned above, uprate of the reactor thermal power up to about 102% is generally feasible just by increasing the measurement accuracy of the feedwater flowmeter 39, etc., and the feedwater temperature is not required to be lowered in such an uprate range. In the boiling water reactor power plant, therefore, the control of the feedwater temperature described in the second to sixth embodiments is more effective when applied to the case of uprating the reactor thermal power in the range of larger than 102%, but smaller than 105%. Further, at the uprate of the nuclear thermal power in the range of 105% to 120%, substantial change of system equipment, e.g., replacement of the high pressure turbine 3, is not required in general. The effects of those embodiments are especially noticeable when applied to the uprate of the reactor thermal power in excess of 105% because the replacement of the high pressure turbine 3 is not required even in the power uprate operation in excess of 105% by employing the power uprating method of lowering the feedwater temperature according to the present invention.
While the second to sixth embodiments have been described in connection with the case where the power uprating method of lowering the feedwater temperature is applied to the boiling water reactor power plant, the following description is made of an example in which the power uprating method is applied to a pressurized water reactor power plant as one of reactor power plants.
The pressurized water reactor power plant according to still another embodiment (seventh embodiment) of the present invention will be described below with reference to
In this seventh embodiment, a steam generator 49 is newly installed in addition to the construction of the second embodiment such that a primary loop and a secondary loop are formed. The primary loop is a circulation loop starting from the reactor pressure vessel 1, passing the steam generator 49, and returning to the reactor pressure vessel 1. The secondary loop is formed by connecting both the main steam system 2 and the feedwater system 23 in the second embodiment to the steam generator 49. The high-temperature coolant generated from the reactor pressure vessel 1 is supplied to the steam generator 49 and is returned to the reactor pressure vessel 1 after the coolant temperature has been lowered. In the steam generator 49, the feedwater supplied from the feedwater system 23 is heated by the high-temperature coolant to become steam. The secondary steam delivered from the steam generator 49 is introduced to the high-pressure turbine 3, the moisture separator and heater 24, and the low-pressure turbine 5 through the main steam line 2. The steam discharged from the low-pressure turbine 5 is condensed by the condenser 6 to become water. This water is fed to the steam generator 49 through the feedwater system 23 in which the low pressure feedwater heater 7, the feedwater pump 8, and the high pressure feedwater heater 9 are disposed. Note that one operation cycle is defined as a period from startup of the reactor to the time at which the reactor is shut down for fuel exchange.
When the reactor thermal power is uprated, the amount of heat exchange in the steam generator 49 is increased substantially proportional to the amount of increase of the reactor thermal power. In order to offset the amount of heat exchange in the steam generator 49, the flow rate of the feedwater supplied to the steam generator 49 has to be increased or the enthalpy difference of the coolant between the inlet and the outlet of the steam generator 49 has to be increased. The known power uprating method employs the former manner; namely it increases the flow rate of the feedwater in proportion to the amount of heat exchange in the steam generator 49. On the other hand, this embodiment employs the latter manner, i.e., the new power uprating method. More specifically, in this embodiment, increases of both the flow rate of the main steam and the flow rate of the feedwater in the power uprate operation are suppressed by intentionally reducing the coolant enthalpy (temperature) at the inlet of the steam generator 49, to thereby increase the enthalpy difference between the inlet and the outlet of the steam generator 49. Thus, this embodiment is adapted for the new power uprating method and requires additional equipment for widening a feedwater temperature controllable range so that the feedwater temperature is lowered to a value beyond the range estimated in the stage of plant construction.
The necessity of widening the feedwater temperature controllable range toward the lower temperature side in turn requires the flow rate of steam extracted for heating the feedwater to be reduced in comparison with that before the power uprate. The extracted steam for heating the feedwater is extracted from the main steam system 2 including the high pressure turbine 3 and the low pressure turbine 5, and is introduced to the high pressure feedwater heater 9 and the low pressure feedwater heater 7 via the extraction lines 25, 26 and 28, etc. In the pressurized water reactor power plant of this embodiment, a plurality of main extraction lines are installed downstream of the inlet of the high pressure turbine and upstream of the outlet of the low pressure turbine. To reduce the flow rate of the extracted steam, an extracted flow control valve 38 is disposed in the extraction line 25 to adjust the flow rate of the extracted steam.
When the above-mentioned new power uprating method of increasing the enthalpy difference of the coolant is employed, it is important that the feedwater temperature be surely lowered to a preset value. For that reason, as in the second embodiment, a feedwater temperature sensor 39 is disposed in the feedwater system 23 downstream of the high pressure feedwater heater 9 that is located most downstream in the feedwater system 23, and the opening of the extracted flow control valve 38 is controlled to adjust the flow rate of the extracted steam. The feedwater temperature sensor 39 is disposed in the feedwater system 23 downstream of the high pressure feedwater heater 9, to which the extracted steam is supplied at the controlled flow rate, and upstream of the inlet of the steam generator 28. As an alternative, the feedwater temperature sensor 39 may be disposed between the high pressure feedwater heater 9, to which the extracted steam is supplied at the controlled flow rate, and another suitable feedwater heater installed downstream of the former. Further, the sensor 39 may be disposed between an outlet of a high pressure feedwater heater installed most downstream and an inlet of the steam generator 49.
One example of control logic executed by the extracted flow controller 40 in the seventh embodiment will be described below with reference to
According to this embodiment, since the feedwater temperature can be adjusted to the set value through control of the opening of the extracted flow control valve 38, it is possible to suppress variations in the amount of power generated during the power uprate operation of the nuclear power plant.
Also, according to this embodiment, since the feedwater temperature can be always held at the set value, it is possible to suppress the increases of both the flow rate of the main steam and the flow rate of the feedwater by lowering the feedwater temperature in the power uprate operation of the reactor. Further, since the feedwater temperature can be adjusted in real time, the operation method of this embodiment is adaptable for the load following operation of the nuclear power plant, as with the second embodiment, while the flow rate of the main steam and the flow rate of the feedwater are held constant.
A pressurized water reactor power plant according to still another embodiment (eighth embodiment) of the present invention will be described below with reference to
As in the third embodiment, this eighth embodiment includes, instead of the feedwater temperature sensor 39, an extraction flowmeter 44 disposed in the extraction line 25 in which the extracted flow control valve 38 is disposed. Comparing with the arrangement of the seventh embodiment that the extracted flow controller 40 controls the extracted flow control valve 38 in accordance with the measured value from the feedwater temperature sensor 39, this eighth embodiment is modified such that the extracted flow controller 40 controls the extracted flow control valve 38 in accordance with the measured value from the extraction flowmeter 44.
The extracted flow control valve 38 and the extraction flowmeter 44 may be disposed in the extraction line 25 irrespective of which one of them is positioned upstream of the other. When the extraction line 25 is merged midway with another extraction line, one of the extracted flow control valve 38 and the extraction flowmeter 44, which is positioned on the downstream side, may be disposed in the extraction line 25 downstream of the merging point between the two extraction lines. Also, when the extraction line 25 is branched midway, one of the extracted flow control valve 38 and the extraction flowmeter 44, which is positioned on the downstream side, may be disposed in a line after being branched. If the reactor thermal power, the flow rate of the feedwater, and the flow rate of the extracted steam are known, the feedwater temperature is uniquely decided from the heat balance of the nuclear power plant.
As in the third embodiment, the extracted flow controller 40 controls the opening of the extracted flow control valve 38 in accordance with the extracted flow measured value signal 45 and the extracted flow set value signal 42A. This eighth embodiment can also provide similar advantages to those obtainable with the seventh embodiment.
A pressurized water reactor power plant according to still another embodiment (ninth embodiment) of the present invention will be described below with reference to
A pressurized water reactor power plant according to still another embodiment (tenth embodiment) of the present invention will be described below with reference to
As in the fifth embodiment, the extracted flow controller 40 receives a main-steam flow measured value signal 47 outputted from the main steam flowmeter 46 and a set value signal 48 for the flow rate of the main steam. Then, the extracted flow controller 40 produces an opening demand signal 43 based on those two signals and controls the extracted flow control valve 38 in accordance with the produced opening demand signal 43. This tenth embodiment can also provide similar advantages to those obtainable with the seventh embodiment.
A pressurized water reactor power plant according to still another embodiment (eleventh embodiment) of the present invention will be described below with reference to
Instead of the above-described arrangement, the main steam flowmeter 46 and the feedwater temperature sensor 39 may be disposed to perform the control based on the flow rate of the main steam and the control based on the feedwater temperature. Further, the main steam flowmeter 46 and the extraction flowmeter 44 may be disposed to perform the control based on the flow rate of the main steam and the control based on the flow rate of the extracted steam.
While the seventh, eighth and tenth embodiments of the present invention have been described, by way of example, in connection with the pressurized water reactor, the present invention can also be applied to an indirect-cycle plant other than the pressurized water reactor.
Generally, when the flow rate of the extracted steam is reduced to lower the feedwater temperature, the thermal efficiency of the plant is reduced. In order to suppress such a reduction of the thermal efficiency, it is preferable to reduce the flow rate of the steam extracted from the extraction point that is positioned as possible as close to uppermost side. In the seventh to eleventh embodiments, therefore, a greater effect can be obtained by installing the extracted flow control valve 38 in the extraction line for extracting the steam from a point downstream of the inlet of the high pressure turbine and upstream of the inlet of the lower pressure turbine. While the extracted flow control valve 38 is disposed only in one extraction line in the seventh to eleventh embodiments, the feedwater temperature cannot be sufficiently lowered in some cases if the flow rate of the extracted steam through only one extraction line is reduced. In such a case, the extracted flow control valve 38 is disposed in plural extraction lines.
In the pressurized water reactor power plant, uprate of the reactor thermal power up to about 102% is generally feasible just by increasing the measurement accuracy of the feedwater flowmeter 39, etc., and the feedwater temperature is not required to lowered in such an uprate range, as mentioned above. In the pressurized water reactor power plant, therefore, the control of the feedwater temperature described in the seventh to eleventh embodiments is more effective when applied to the case of uprating the reactor thermal power in the range of larger than 102%, but smaller than 105%. Further, at the uprate of the nuclear thermal power in the range of 105% to 120%, substantial change of system equipment, e.g., replacement of the high pressure turbine 3, is not required in general. The effects of those embodiments are especially noticeable when applied to the uprate of the reactor thermal power in excess of 105% because the replacement of the high pressure turbine 3 is not required even in the power uprate operation in excess of 105% by employing the power uprating method of lowering the feedwater temperature according to the present invention.
Number | Date | Country | Kind |
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2005-021835 | Jan 2005 | JP | national |
2005-066498 | Mar 2005 | JP | national |
This application is a divisional application of U.S. application Ser. No. 12/574,219 filed Oct. 6, 2009, which is a divisional application of U.S. application Ser. No. 11/340,643, filed Jan. 27, 2006, now U.S. Pat. No. 7,614,233, the entirety of which are incorporated herein by reference. The present application claims priority from Japanese Patent Application No. 2005-021835, filed Jan. 28, 2005 and 2005-066498, filed Mar. 10, 2005, the contents of which are incorporated herein by reference.
Number | Date | Country | |
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Parent | 12574219 | Oct 2009 | US |
Child | 13046294 | US | |
Parent | 11340643 | Jan 2006 | US |
Child | 12574219 | US |