Propulsion systems have been improved by scientists, researchers, engineers as well as manufacturers to the present state of the art of fluid or air propellers, It is well known the propeller slipstream disc contracts between 0.816 to 0.92 depending on the propeller forward velocity from zero and low forward speed, and the contraction occurs near the outer edge of the propeller disc, Static Propellers & Helicopter Rotors, AHS 25th Forum 1969, and Fluid-Dynamic Lift, Chapter XII, S. F. Hoerner, and H. V. Borst, Second Edition, published by Liselotte A. Hoerner, 1985, 7628 Staunton Place, N. Mex. 87120. It has been suggested propeller disc contraction has not been completely addressed. Airfoils have been designed to reduce trailing vortices, Chapter III, and Chapter XII
The present invention relates to using the state of the art propeller containing an internal passage that connects a leading edge inlet slot and a trailing edge exit slot, allowing the fluid or air entering the propeller at approximately ninety degrees by way of the leading edge slot to be acted upon and forced out of the trailing edge propeller tip by centrifugal force varying directly as the speed of the propeller rotation. The exit trajectory of the fluid or air is parallel to the cambered face of the propeller and at approximately forty-five degrees to the longitudinal axis of the propeller. The velocity and capacity of the fluid or air varies directly as the speed of rotation.
It is an object of the invention to provide a method of propeller propulsion with less propeller slipstream disc contraction, thus producing more thrust and efficiency.
It is an object of the invention that the exiting fluid or air from the trailing edge exit induces flow over the cambered face of the propeller apparatus, adds an amount of bootstrapping to the capacity if the propeller, and by the jetting of the exiting fluid or air causes the propeller to turn more easily.
It is also another object of the invention to provide a method of propeller propulsion to improve the propeller propulsion efficiency.
These objects and others are achieved in accordance with this invention which embodies, a propeller either solid with a passage connecting or hollow core, with an inlet on the leading edge some distance or approximately twenty percent of the propeller diameter measured from the propeller tip to an exit slot on the trailing edge of the propeller tip having the fluid or air exiting parallel to the cambered face of the propeller and at approximately forty-five degrees to the longitudinal axis of the propeller.
The characteristics of the preferred device and its principle of operation, will be more fully understood by reference to the following more detailed description, and the attached drawings to which reference is made. The various components of the device, a propeller, are referred to in terms of reference numerals and letters, similar numbers being used in the different figures to designate components. In describing certain components, and features thereof, subscripts have been used with whole numbers for convenience to describe subcomponents of a different part.
The invention will now be described in connection with the accompanying drawings:
The following examples and demonstrations exemplify the augmented propeller of this invention; comparative data being presented to demonstrate the advantage in improved thrust and efficiency achieved pursuant to the practice of this invention.
Prior flight tests were made in a Wittman 125 horsepower retractable gear monoplane to obtain data of the magnitude of the slipstream disc contraction of a propeller driven airplane at airspeeds of a 160 miles per hour. The airplane was equipped with a fixed pitch 68/75 propeller and further equipped with a an airspeed indicator and pitot system mounted in the propeller slipstream taking airspeed readings approximately 6 inches to the rear of the propeller. The pitot tube was moved in increments of one inch starting at the tip of the propeller after each test flight flown at 160 miles per hour. The slipstream contraction was measured to be approximately 6 inches for 68 inch diameter propeller or approximately 0.911, which is reasonable compared to the studies by S. F. Horner and H. N. Borst reference above. These results demonstrated a reduction of the slipstream disc contraction of the test aircraft would increases the flow of air at the propeller tips, and is a viable subject for improvement in performance and efficiency as the following tests below demonstrate.
Tests of 10 inch diameter two bladed 10/6 propellers manufactured by JZ Zinger Company were performed on a dynamometer. The first propeller tested, marked as the control propeller, was covered with a thin veneer 1 on the back side 12 opposite the propeller cambered face 11. The second test propeller back 12 was modified by carving a channel 9 between the inlet 7 at the leading edge 5 and the tip outlet 8 at the trailing edge 4, the inlet 7 on the leading edge 5 measures approximately twenty percent of the diameter from the tip. Flow from the inlet slot 7 located of the leading edge 5 allows flow to the outlet at the trailing edge 8 tip wherein flow is directed 14 parallel to the camber propeller face 11 and at an angle of approximately forty-five degrees 17 to the longitudinal axis of the propeller. The back 12 of the second test propeller was carved out and covered with a thin veneer 1, creating a direct passage 9 between the inlet slot 7 and outlet slot 8 of minimum size. The third test propeller was also modified by carving an internal passage creating a larger hollow core 9 after also being covered with a thin veneer 1. Except for the size of the internal passage 9 between the inlet 13 to the outlet 14,
Demonstration One: The control propeller provided an average 1175 grams thrust reading for an input of 4 amps at 8265 rpm.
Demonstration Two: The second propeller provided an average 1205 grams thrust reading for an input of 4 amps at 8230 rpm.
Demonstration Three: The third propeller provided an average of 1226 grams thrust reading for an input of 4 amps at 8270 rpm.
There is a 4.3 percent improvement of thrust of the control propeller by the third propeller.
Subsequent tests were made with the control propeller and third propeller since the third propeller internal passage was of sufficient capacity, hollow core, as demonstrated to have an increase in thrust readings, induced flow over the propeller apparatus camber 18, as well as having an average increase in rpm. The subsequent tests as recorded in
It is apparent that various modifications and changes can be made without departing from the spirit and scope of the present invention. Changes in absolute dimensions of the parts, materials of construction used, and the like will be apparent to those skilled in the art.